N7VX

Substantial
Serious

WALTON VELOCITY STD/FG S/N: DMO46

Accident Details

Date
Monday, August 25, 1997
NTSB Number
LAX97LA304
Location
CHINO VALLEY, AZ
Event ID
20001208X08690
Coordinates
34.769721, -112.449203
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

a loss of engine power for undetermined reasons.

Aircraft Information

Registration
N7VX
Make
WALTON
Serial Number
DMO46
Model / ICAO
VELOCITY STD/FG

Registered Owner (Historical)

Name
WALTON MOSES
Address
530 BRADSHAW DR
Status
Deregistered
City
PRESCOTT
State / Zip Code
AZ 86303-5808
Country
United States

Analysis

On August 25, 1997, at 1215 hours mountain standard time, a Walton Velocity STD/FG experimental aircraft, N7VX, collided with terrain following a loss of power due to fuel starvation at Chino Valley, Arizona. The aircraft sustained substantial damage. The private pilot, the sole occupant, received serious injuries. The aircraft was being operated as a personal flight under 14 CFR Part 91 when the accident occurred. The flight originated in Winslow, Arizona, at 1050. Visual meteorological conditions prevailed at the time of the accident.

The pilot stated that he was about 20 miles from Sedona when he noticed the engine surging. He said that he tried both magnetos with no luck. He also said he checked the throttle to readjust the mixture and tried the secondary electric fuel pump, which straightened out the problem for a few minutes. As he was looking for a place to land, the engine quit and he tried to land down a dirt road but collided with some scrub oaks.

In his initial report to the Federal Aviation Administration Prescott Flight Service Station, the pilot said that something had gone wrong with the fuel line, thus leading to the fuel starvation of the engine. In his written report to the Safety Board, he said he thought it must have been some sort of fuel starvation problem because the gauges showed that the aircraft was almost full of fuel.

The aircraft was retrieved from the accident site and brought to the Air Transport facility in Phoenix, Arizona, for further examination. The pilot's insurance adjuster arranged for guard service on the aircraft overnight following the accident and prior to the retriever's arrival. The individuals who were guarding the aircraft stripped off all instrumentation and avionics equipment. In addition, the wings and fuel system had been disassembled prior to the retriever's arrival.

The aircraft was examined under the direction of the Safety Board. The engine manufacturer stated the engine was first observed attached to the airframe and appeared undamaged by any pre-mishap mechanical malfunction. The aircraft electrical system was powered by a jumper battery in an attempt to run the engine. The engine was observed to operate in a normal manner with no unusual sounds or vibrations noted. Both magnetos operated normally when the magneto switch was selected from right to left and back to both. There was no instrumentation in the cockpit to record any parameters during the run-up examination.

The Safety Board did not to take custody of the wreckage.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX97LA304