N71585

Substantial
Serious

LUSCOMBE 8A S/N: 3012

Accident Details

Date
Wednesday, September 1, 1993
NTSB Number
ANC93LA165
Location
KIJIK RIVER, AK
Event ID
20001211X13285
Coordinates
60.199241, -154.280532
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

THE PILOT'S FAILURE TO MAINTAIN A PROPER ALTITUDE DURING THE LOW PASS.

Aircraft Information

Registration
N71585
Make
LUSCOMBE
Serial Number
3012
Engine Type
None
Year Built
1946
Model / ICAO
8A L8
No. of Engines
0

Registered Owner (Historical)

Name
MOULTON KATHERINE L
Address
7161 BEAUMONT CIR
Status
Deregistered
City
ANCHORAGE
State / Zip Code
AK 99502
Country
United States

Analysis

On September 1, 1993, at 1500 Alaska daylight time, the pilot of a wheel equipped Luscombe 8A airplane, N71585, lost control of the airplane and crashed while maneuvering in a mountain valley near the Kijik River, approximately 30 miles northeast of Port Alsworth, Alaska. The commercial pilot, the sole occupant, received serious injuries, and the airplane was substantially damaged. The personal flight, operating under 14 CFR Part 91, departed Port Alsworth at about 1415, with a destination of the Stony River Lodge. Visual meteorological conditions existed, and no flight plan was filed.

During a telephone interview on September 3, 1993, the pilot stated the following, in part: "I was trying to follow the map and fly through the mountains. I was not familiar with the area and had never flown that route before. I had flown through one little pass, then realized that I had gone the wrong way and was too far east. I saw a valley heading to the west so I decided to fly that way. I could see a saddle at the end and over into another valley. I had added power, but realized that the airplane wasn't going to climb high enough in time to get over the saddle, so I decided to turn around and get out. During the turn I didn't notice that the airspeed had got so slow. The airplane suddenly stalled and went into a spin. I might have got into a downdraft. I was pretty close to the ground, but managed to pull the nose up and get out of the spin and into a pretty level attitude. The airplane pancaked in right at the bottom of the pull up and the fuselage broke in half."

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ANC93LA165