N5647X

Destroyed
Minor

Aero Commander S2R S/N: 1847R

Accident Details

Date
Friday, March 19, 1999
NTSB Number
FTW99LA097
Location
HOBART, OK
Event ID
20001205X00325
Coordinates
35.019214, -99.089546
Aircraft Damage
Destroyed
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
0
Total Aboard
1

Probable Cause and Findings

The loss of engine power due to an undetermined reason. A factor was the ditch.

Aircraft Information

Registration
N5647X
Make
AERO COMMANDER
Serial Number
1847R
Engine Type
Turbo-jet
Year Built
1973
Model / ICAO
S2R L29
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
BURNETTE NORMAN L DBA
Address
PO BOX 1152
Status
Deregistered
City
WYNNE
State / Zip Code
AR 72396
Country
United States

Analysis

On March 19, 1999, at 1720 central standard time, an Aero Commander S2R, agricultural airplane, N5647X, struck a ditch during an aborted takeoff following a loss of engine power. The airplane was owned by Burnette Flying Service at Wynne, Arkansas, and operated by AFS Spraying Service, Hobart, Oklahoma, under 14 Code of Federal Regulations (CFR) Part 137. The commercial pilot, sole occupant, received minor injuries. The airplane was destroyed by a fire. Visual meteorological conditions prevailed and a flight plan was not filed for the local aerial application flight. The flight was originating at the time of the accident.

Local authorities and the FAA inspector reported that during the takeoff there was a loss of engine power. The airplane struck a ditch and the main landing gear collapsed. The airplane slid to a stop and the pilot exited the cockpit prior to the fire destroying the airplane.

During a telephone interview, conducted by the investigator-in-charge (IIC), the pilot reported that the airplane had experienced a loss of engine power on March 17, 1999, and he had executed an emergency landing in a field. He assessed that it was "possibly a carburetor float or seat sticking". On March 19, 1999, he replaced the carburetor and restarted the engine. There were no discrepancies found during the ground check; however, "at lift off speed the engine backfired smoke and flame from the exhaust port." The pilot shut down the engine and braked to a stop. While exiting the aircraft, the pilot noticed black smoke coming from the accessory compartment.

The airplane was examined by the FAA inspector and the operator. Fire damage prevented a determination of a cause for the loss of engine power.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# FTW99LA097