N8883M

Substantial
None

Beech A23 S/N: M632

Accident Details

Date
Sunday, March 28, 1999
NTSB Number
MIA99LA115
Location
HOMESTEAD, FL
Event ID
20001205X00370
Coordinates
25.529331, -80.389320
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The pilots improper decision not to land straight ahead after sustaining a reported loss of engine power on initial take off climb with sufficient runway remaining, and improper recovery from a bounced landing resulting in a subsequent in-flight collision with terrain. The reported loss of engine power was not determined.

Aircraft Information

Registration
N8883M
Make
BEECH
Serial Number
M632
Engine Type
Reciprocating
Year Built
1964
Model / ICAO
A23 BE23
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
MATHIS PAINT AND BODY
Address
100 149 OVERSEAS HWY
Status
Deregistered
City
KEY LARGO
State / Zip Code
FL 33037
Country
United States

Analysis

On March 28, 1999, about 1006 eastern standard time, a Beech A23, N8883M, registered to Mathis Paint and Body, operating as a 14 CFR Part 91 personal flight, crashed on initial climbout from Homestead General Aviation Airport, Homestead, Florida. Visual meteorological conditions prevailed and no flight plan was filed. The airplane sustained substantial damage. The private pilot and one passenger reported no injuries. The flight was originating at the time of the accident.

The pilot stated he departed from runway 09. "At approximately 60 feet above the field the engine loss power and vibrated extremely....I then made a poor judgement call and turned the plane into a 45 degree angle. After the rollout I saw a clearing and headed for it." The right main landing gear touched down, the airplane bounced to the left striking the wing tip and landing left landing gear, before the airplane skidded to a stop.

The FAA stated, "the overall condition of the engine appeared to be poor. Many spark plugs were badly rusted, hoses, wiring, and accessories appeared to be old and in need of inspection." The airplane was examined by an airframe and powerplant mechanic. The propeller was pulled through and compression was present. The crankshaft and propeller moved freely.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# MIA99LA115