N22RQ

Destroyed
None

REINDL QUICKIE 2 S/N: 2118

Accident Details

Date
Sunday, April 11, 1999
NTSB Number
CHI99LA127
Location
OLATHE, KS
Event ID
20001205X00437
Aircraft Damage
Destroyed
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The loss of engine power for undetermined reasons. A factor associated with the accident is the lack of suitable terrain for a forced landing.

Aircraft Information

Registration
N22RQ
Make
REINDL
Serial Number
2118
Model / ICAO
QUICKIE 2

Registered Owner (Historical)

Name
PECK NATHAN M
Address
9111 SANTA FE LN APT 202
Status
Deregistered
City
OVERLAND PARK
State / Zip Code
KS 66212-3770
Country
United States

Analysis

On April 11, 1999, at 1449 central daylight time, an amateur-built Reindl Quickie 2, N22RQ, was destroyed during a forced landing following a partial loss of engine power during take-off from the New Century Aircenter Airport, near Olathe, Kansas. The pilot executed the forced landing to a plowed farm field. Visual meteorological conditions prevailed at the time of the accident. The personal flight was conducted under 14 CFR Part 91. There was no flight plan on file. The pilot reported no injuries to himself or to his one passenger. The local flight was originating at the time of the accident.

In a written statement, the pilot stated that the engine was producing full power at the start of the takeoff roll. The pilot stated that he had reached an altitude of 100 to 200 feet when he realized that he was losing power. The pilot stated that, during the descent and eventual forced landing, "the engine continued to run smooth without any roughness." The pilot stated that he believes the loss of power was due to the "engine-carburetor combination."

At a post accident examination, the engine was found separated from the firewall, the engine was found to have compression, the continuity of the valve train and the accessory drives was confirmed, and no water was found in the fuel system. The carburetor was found separated from the engine and was damaged. The pilot reported that he had obtained fuel prior to the accident flight and fuel was found at the accident scene. No evidence of fuel contamination was found. No pre-existing anomalies were found regarding the airframe, and none were reported by the pilot.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI99LA127