N869M

Substantial
Serious

INMAN ACRO SPORT 1 S/N: 357

Accident Details

Date
Saturday, July 23, 1994
NTSB Number
CHI94LA243
Location
ALBERT LEA, MN
Event ID
20001206X01711
Coordinates
43.650299, -93.359680
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

the pilot's failure to make a precautionary landing on the remaining runway. Factors in the accident were the blocked fuel injector and inadvertent stall.

Aircraft Information

Registration
N869M
Make
INMAN
Serial Number
357
Model / ICAO
ACRO SPORT 1

Registered Owner (Historical)

Name
WILLKOMM JOHN C
Address
7510 88 AVE
Status
Deregistered
City
KENOSHA
State / Zip Code
WI 53142
Country
United States

Analysis

On July 23, 1994, at 1530 central daylight time, an Acro Sport, N869M, sustained substantial damage when it made a hard landing after losing engine power immediately after taking off from Albert Lea Municipal Airport, Albert Lea, Minnesota. The private pilot, who was participating in an acrobatic competition at the time of the accident, received serious injuries. The 14 CFR Part 91 flight operated in visual meteorological conditions.

According to one witness, N869M departed runway 34 (4501' x 100') and leveled off approximately 150 feet above the ground and 1200 feet down the runway. At the same time that the airplane leveled off, the witness states he heard a reduction in engine power. When the airplane reached the end of runway 34, he observed the airplane make a steep to medium bank to the left. The witness did not see the airplane impact the ground, but does state that he did not hear any backfiring. The airplane was at reduced power, and stayed at the same RPM the entire time that he was able to hear the engine.

A second witness first noticed the airplane shortly after takeoff, level at approximately 150 feet above the ground and operating at reduced power. The witness states that the pilot had approximately 2600 feet of runway remaining at the time when he leveled off. He states there was no indication of a rough running engine or any visible smoke. The witness states he expected the airplane to land on the remaining runway, but the airplane continued. He then states that the pilot initiated a left turn while maintaining altitude. At the conclusion of the turn, at approximately 75 feet above the ground, the witness observed the airplane's nose pitch down slightly, the sink rate increased dramatically, and the right wing dropped slightly. The aircraft impacted the ground in a 15 degrees nose down attitude. The witness states there was no change in engine sound throughout the occurrence.

A postaccident inspection of the engine revealed the number three fuel injector was plugged with a small amount of an unidentified matter.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI94LA243