N63VW

Destroyed
Fatal

LAFRANCE V-WITT W2 S/N: 37

Accident Details

Date
Saturday, August 20, 1994
NTSB Number
BFO94LA141
Location
WILMINGTON, OH
Event ID
20001206X01965
Coordinates
39.440128, -83.830116
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
1
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

LOSS OF ENGINE POWER FOR AN UNDETERMINED REASON, AND FAILURE OF THE PILOT TO MAINTAIN ADEQUATE AIRSPEED WHILE ATTEMPTING A MANEUVER FOR AN EMERGENCY LANDING, WHICH RESULTED IN A STALL AND COLLISION WITH TERRAIN. A FACTOR RELATED TO THE ACCIDENT WAS: THE LACK OF ALTITUDE FOR REMEDIAL ACTION (AFTER LOSS OF ENGINE POWER).

Aircraft Information

Registration
N63VW
Make
LAFRANCE V-WITT
Serial Number
37
Model / ICAO
W2

Registered Owner (Historical)

Name
MCCOWN MARK S
Address
983 HYROCK BLVD
Status
Deregistered
City
BOONVILLE
State / Zip Code
IN 47601-9571
Country
United States

Analysis

On August 20, 1994, at 1803 eastern daylight time, N63VW, a homebuilt V-WITT W2, operated by the private pilot/registered owner, crashed at Wilmington, Ohio. The private pilot, the sole occupant, was fatally injured. The airplane was destroyed. Visual meteorological conditions prevailed and a flight plan was not filed. The local, personal flight was operated under 14 CFR 91.

According to an FAA Aviation Safety Inspector, the pilot was performing in an airshow. He stated that the pilot had completed his preflight inspection and had some problems starting the engine. He stated that the pilot started the engine, completed an engine run-up and departed on runway 22. He stated the pilot completed his performance and returned to the airfield.

Witnesses stated they observed the airplane circling the field. One witness stated that the airplane, "...seemed from my angle to climb slightly, level the wings, then all of a sudden the left wing appeared to drop, the airplane went into a left bank, and then the nose dropped." Another witness stated that he heard the engine sputter and, "...it appeared to lose power."

The airplane was examined at the accident site by an FAA Inspector. The examination revealed the fuel selector valve which has two positions, "on" and "off", was found in the off position. The FAA Inspector reported that he asked the rescue team if anyone had switched the fuel off and he was told that no one touched anything in the airplane. The FAA Inspector reported there was no evidence of preimpact mechanical malfunction.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# BFO94LA141