N45LW

Substantial
None

HERRON LITTLE WING AUTOGYROS/N: LW-1

Accident Details

Date
Friday, October 21, 1994
NTSB Number
FTW95LA031
Location
LITTLE ROCK, AR
Event ID
20001206X02451
Coordinates
34.840507, -92.330558
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

THE FRACTURED TAIL WHEEL MOUNTING BRACKET AND LOOSE TAILWHEEL. A FACTOR WAS THE PILOT'S CONTINUED FLIGHT TESTING AFTER EXPERIENCING TAIL WHEEL SHIMMY ON THE PRIOR TEST FLIGHT.

Aircraft Information

Registration
Make
HERRON
Serial Number
LW-1
Engine Type
Reciprocating
Year Built
1994
Model / ICAO
LITTLE WING AUTOGYROBPAT
Aircraft Type
Rotorcraft
No. of Engines
1
Seats
2
FAA Model
LITTLE WING AUTOGYRO

Registered Owner (Current)

Name
RAZORBACK ROTORS INC
Address
108 W 13TH ST STE 105
City
WILMINGTON
State / Zip Code
DE 19801-1145
Country
United States

Analysis

On October 21, 1994, at 1500 central daylight time, a Herron Little Wing Autogyro, N45LW, was substantially damaged while landing near Little Rock, Arkansas. The private pilot was not injured. Visual meteorological conditions prevailed for the local test flight.

The pilot, and builder of the gyroplane, was conducting initial low level flight and taxi tests at North Little Rock Municipal Airport. He stated that the "initial flight tests" consisted of climbs, descents, and S-turns conducted at low altitude over the runway surface. Both hovering and roll-on landings were conducted with power on. These were accomplished by taking off from the approach end of the runway, flying the length of the runway at low altitude, and landing the airplane at the departure end. This sequence was accomplished 10 or 12 times with no problems. The pilot stated that, during the last landing, he attempted to land the gyroplane with power off and 10 to 15 knots of forward airspeed. The initial touchdown was on the two front main landing gear, and as the tail wheel came in contact with the ground, the tail turned sharply to the right. The aircraft then swerved to the left and rolled inverted to the right causing structural damage.

After the accident, the pilot reported that the aircraft had a "tail wheel shimmy" during ground taxi testing the day prior to the accident. Examination of the aircraft after the accident revealed that the mounting bracket for the tail wheel assembly was fractured for undetermined reasons, and the tail wheel was loose.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# FTW95LA031