N701AM

Substantial
None

CESSNA 421B S/N: 80366

Accident Details

Date
Monday, October 3, 1994
NTSB Number
MIA95LA002
Location
STUART, FL
Event ID
20001206X02489
Coordinates
26.850036, -80.090988
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
7
Total Aboard
7

Probable Cause and Findings

THE IMPROPER RIGGING OF THE LANDING GEAR SAFETY SQUAT SWITCH BY OTHER MAINTENANCE PERSONNEL. CONTRIBUTING TO THE ACCIDENT WAS THE CONTAMINATION OF THE GEAR SQUAT SWITCH WITH CORROSION AND WATER.

Aircraft Information

Registration
Make
CESSNA
Serial Number
80366
Engine Type
Reciprocating
Year Built
1973
Model / ICAO
421B C421
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2
Seats
8
FAA Model
421B

Registered Owner (Current)

Name
QUEST AVIATION INC
Address
173 SE NEWELL DR
City
LAKE CITY
State / Zip Code
FL 32025-1986
Country
United States

Analysis

On October 3, 1994, about 0753, eastern daylight time, N701AM, a Cessna C-421B, registered to and operated by Air Mobile Ministries, experienced an all-landing gears collapse on landing at Whitman Field, Stuart, Florida. The flight was a 14 CFR Part 91 personal flight. The planned destination was Port-au-Prince, Haiti. Visual meteorological conditions prevailed at the time and a VFR flight plan was filed. The airplane was substantially damaged and the pilot and six passengers reported no injuries. The flight was originating at the time of the accident.

The pilot stated that after takeoff the landing gear would not come up so he placed the gear handle in the down position and observed three green lights. On landing roll the gear collapsed. The one passenger who was on board was an FAA employee in a duty travel status, from the San Juan, Puerto Rico, Flight Standards District Office.

Examination of the landing gear safety switch [Squat] by FAA personnel revealed that the switch was corroded, full of water and was improperly rigged. FAA personnel also reported the airplane weight and balance data used by the pilot for takeoff computations was in error, and the airplane was about 200 pounds over gross weight on departure.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# MIA95LA002