N8903G

Substantial
None

CESSNA 182N S/N: 182-60443

Accident Details

Date
Saturday, October 8, 1994
NTSB Number
NYC95LA004
Location
NEW LONDON, NH
Event ID
20001206X02505
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

the failure of the number four push rod, which resulted in the complete loss of engine power and forced landing, and the subsequent nose over on soft terrain.

Aircraft Information

Registration
N8903G
Make
CESSNA
Serial Number
182-60443
Engine Type
Reciprocating
Model / ICAO
182N C182
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
WHEELER JAMES P
Address
PO BOX 981
Status
Deregistered
City
NEW LONDON
State / Zip Code
NH 03257
Country
United States

Analysis

On October 8, 1994, at 1700 eastern daylight time, a Cessna 182N, owned and piloted by James P. Wheeler, was substantially damaged during a forced landing to an open field, near the New London Airport, New London, New Hampshire. The pilot received minor injuries. Visual meteorological conditions prevailed and no flight plan had been filed for the flight operating under 14 CFR 91.

In the NTSB 6120.1/2, the pilot stated he had departed Springfield, Vermont, with full fuel tanks for a flight to Eagles Nest Airport, New London, New Hampshire. Thirty minutes after takeoff, and approximately 3 miles from the Eagles Nest Airport, the engine began to run rough with violent backfiring. He further stated:

"...It failed completely approximately 60 seconds later and I executed an emergency landing in an open field. The ground was soft and slightly wet and the nose wheel dug in enough to break. The aircraft slid on its wheels for approximately 75 feet before slowing and tipping over inverted (nose over)..."

A Federal Aviation Administration (FAA) Inspector interviewed the pilot and summarized a statement. In the summary, the pilot stated that he was level at 2200 feet, a few miles from the destination airport when the engine lost power. He continued in a southeasterly direction toward the airport when the engine failed completely. The pilot selected a field, turned a low base to final, and made a "very hard" no flap landing to the northwest.

The airplane was removed to a local airport and the engine was started for a test run. In the FAA Inspector's report, it stated:

"...The engine started but ran very rough...The number four exhaust valve push rod was found to be broken (it was bent and severely worn)...The failed pushrod would have resulted in engine operating conditions similar to those described by the pilot...The failed pushrod was bent and severely worn prior to the failure. There was no evidence of any wear on the inside of the pushrod housing. The number four cylinder was removed and everything except for the pushrod appeared normal..."

The airplane records revealed that the engine had been overhauled within the last 90 flight hours.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# NYC95LA004