N3983H

Substantial
None

MOONEY M20K S/N: 25-0387

Accident Details

Date
Wednesday, December 28, 1994
NTSB Number
CHI95LA058
Location
MINNEAPOLIS, MN
Event ID
20001206X02702
Coordinates
44.879371, -93.199073
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

the pilot's misjudging of distance and airspeed during the approach to landing which resulted in an overrun. Factors associated with the accident were the separation of the exhaust pipe and the pilot's not understanding communications from the air traffic control tower.

Aircraft Information

Registration
N3983H
Make
MOONEY
Serial Number
25-0387
Engine Type
Reciprocating
Year Built
1980
Model / ICAO
M20K M20T
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
MIDWEST MOONEY LLC
Address
2 AIRPORT RD
Status
Deregistered
City
FLORA
State / Zip Code
IL 62839-3450
Country
United States

Analysis

On December 28, 1994, about 1517 central standard time, a Mooney M20K, N3983H, sustained substantial damage in a precautionary landing at the Crystal Airport, Minneapolis, Minnesota, when it departed the end of runway 23R, and struck the airport perimeter fence. Neither the commercial pilot, nor the single passenger aboard the airplane were injured. The flight had just departed the Crystal Airport with an intended destination of Rockford, Illinois. An IFR flight plan was filed, and visual meteorological conditions prevailed at the time.

The pilot stated that at an altitude of approximately 200 feet agl, after takeoff, the engine started running rough and an "significant loss of power" occurred. The pilot declared and emergency and was cleared to land on runway 23R. The pilot was later cleared to land on any runway. The pilot stated he, "Did not fully realize all runway[s] were available." He set up for a landing on runway 23R. He stated he was not set up properly, being too close, but decided to land anyway. The airplane touched down long on the runway, traveled off the end and contacted an airport perimeter fence.

A post accident engine test run was conducted. The engine ran up to 2700 rpm without interruption. The only anomaly noted on the was that the #6 cylinder exhaust pipe had separated near the mounting flange.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI95LA058