N9672W

Substantial
Serious

PIPER PA-28-140 S/N: 28-23136

Accident Details

Date
Saturday, May 13, 1995
NTSB Number
BFO95LA053
Location
DUBOIS, PA
Event ID
20001207X03416
Coordinates
41.020931, -78.430900
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
2
Minor Injuries
0
Uninjured
0
Total Aboard
2

Probable Cause and Findings

The failure of valve springs in the number two engine cylinder which resulted in a total loss of engine power during initial climb. The unsuitable terrain encountered during the subsequent forced landing was a factor.

Aircraft Information

Registration
N9672W
Make
PIPER
Serial Number
28-23136
Engine Type
Reciprocating
Year Built
1967
Model / ICAO
PA-28-140 P28A
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
SALE REPORTED
Address
411 AVIATION WAY
Status
Deregistered
City
FREDERICK
State / Zip Code
MD 21701-4756
Country
United States

Analysis

On May 13, 1995, at 1050 eastern daylight time, a Piper PA-28- 140, N9672W, lost total engine power during takeoff climb from runway 25 at the Dubois-Jefferson County Airport, Dubois, Pennsylvania. A forced landing was made in a field near the airport. The pilot and passenger were seriously injured. The airplane was substantially damaged. Visual meteorological conditions prevailed. The local personal flight was conducted under 14 CFR Part 91.

The pilot reported that shortly after takeoff, at an altitude of about 2,800 feet mean sea level, the engine lost power. The pilot wrote, "Heard a loud 'pop' then the engine went from full power to idle. Was going back to (N97). Picked out a farmer's field and went for it. Hit plowed area [and] turned over."

Witnesses stated that they heard the airplanes engine "sputtering" and "cutting out" prior to its touchdown on the field.

Postaccident examination revealed the airplane touched down on a soft, soil field. The airplane nosed over damaging the outboard section of the left wing, vertical fin, rudder, nose gear, nose gear cowling, engine mount, and fuselage skin. Fuel was found throughout the airplane's fuel system.

The airplane and engine were transported to a storage facility for further examination. According to a Federal Aviation Administration Safety Inspector, "Postaccident examination of the engine revealed that the two intake valve springs in the number two cylinder had failed." The inspector stated that the valve spring fracture surfaces were "corroded and pitted."

According to the airplane's owner, the engine had accumulated 13.7 hours since it received a major overhaul.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# BFO95LA053