N3065E

Substantial
None

CESSNA 172N S/N: 172-71425

Accident Details

Date
Thursday, June 1, 1995
NTSB Number
BFO95LA054
Location
HEAD WATERS, VA
Event ID
20001207X03628
Coordinates
38.369365, -79.380294
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
3
Total Aboard
3

Probable Cause and Findings

the pilot's poor planning/decision making in the attempted departure. Contributing factors are the wet, recently mowed grass airstrip, and the embankment/downhill grade encountered during the aborted takeoff.

Aircraft Information

Registration
Make
CESSNA
Serial Number
172-71425
Engine Type
Reciprocating
Year Built
1978
Model / ICAO
172N C172
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
172N

Registered Owner (Current)

Name
3065E LLC
Address
121 PRITCHARD HOLLOW RD
City
WESTFIELD
State / Zip Code
PA 16950-1416
Country
United States

Analysis

On June 1, 1995, at 1730 eastern daylight time, a Cessna 172N, N3065E, was substantially damaged during an aborted takeoff from a private airstrip in Head Waters, Virginia. The commercial pilot and the two passengers were not injured. Visual meteorological conditions prevailed. The personal flight was conducted under 14 CFR Part 91, and the intended destination was Manassas, Virginia.

According to a Federal Aviation Administration Safety Inspector, the pilot and passengers departed Manassas to view some property for sale at Head Water. The pilot stated that he landed the airplane on a field which had been a private airstrip years ago. A witness on the ground stated that at the time N3065E landed, the grass was about 12 inches high. The witness stated at the pilot's request he mowed a portion of the field prior to the attempted takeoff.

The pilot reported on his Safety Board Pilot Aircraft Accident Report form, "Performed a soft/short field take off procedure using 10 [degrees] of flaps. As aircraft became airborne it didn't seem to be developing full power....Aborted takeoff going over embankment at end of runway."

According to the FAA Safety Inspector, during an interview with the pilot after the accident, the pilot stated that during the takeoff roll he thought the engine lost about 100 to 150 revolutions per minute. The pilot stated he aborted the takeoff about 1,000 feet down the 1,500 foot long, wet, grass airstrip. He stated he steered the airplane into taller grass in attempt to "...assist the braking action." The pilot said that the airplane "...appeared to almost be stopped, but went down a 4 foot-high embankment at the end of the airstrip." The pilot stated that while rolling down the embankment, the airplane's nose gear collapsed and the airplane nosed down. The left wing contacted the ground damaging the wing's strut.

Postaccident examination of the accident site revealed the airstrip to be a portion of a mowed grass field with the surrounding grass being about 12 inches high. The mowed section of the field was about 20 feet wide and 1,500 feet long. The mowed grass was not removed. About 1,200 feet down the mowed strip there were three ground marks that departed the mowed strip and continued through the taller grass down an embankment.

Postaccident examination of the airframe and engine did not reveal any anomalies.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# BFO95LA054