N5654X

Substantial
None

AERO COMMANDER S2R S/N: 1854R

Accident Details

Date
Thursday, July 6, 1995
NTSB Number
FTW95LA282
Location
NEWPORT, AR
Event ID
20001207X03943
Coordinates
35.619735, -91.229980
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

A DISCONNECTED THROTTLE PUSH PULL ROD, DUE TO INADEQUATE MAINTENANCE. A FACTOR RELATING TO THE ACCIDENT WAS: THE LACK OF SUITABLE TERRAIN FOR THE FORCED LANDING.

Aircraft Information

Registration
N5654X
Make
AERO COMMANDER
Serial Number
1854R
Engine Type
Turbo-jet
Year Built
1973
Model / ICAO
S2R L29
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
NU LOOK INC
Address
RT 3 BOX 466
Status
Deregistered
City
NEWPORT
State / Zip Code
AR 72112
Country
United States

Analysis

On July 6, 1995, at 1430 central daylight time, an Aero Commander S2R, N5654X, was substantially damaged during a forced landing near Newport, Arkansas. The commercial pilot was not injured. Visual meteorological conditions prevailed for the 14 CFR Part 137 aerial application flight operated by Nu-Look, Inc. The flight originated at 1425 in Newport, Arkansas, and no flight plan was filed.

The pilot stated, in the enclosed Pilot/Operator Report (NTSB Form 6120.1/2), that during "turnaround" from his third pass of fertilizing a rice field, the aircraft "shuddered slightly" followed by a drop in manifold pressure. He "increased power and prop pitch to full forward" and began dumping his load of dry fertilizer as he "started for the private airstrip about one mile away." The pilot further reported that the aircraft could not maintain altitude so he executed a forced landing to a field. The "airplane slid approximately 100 feet, hit [a] rice levee, pitched up onto [its] nose, then fell back onto [its] belly" and caught on fire.

A post crash examination of the aircraft by a Federal Aviation Administration inspector revealed that the throttle control push pull tube, P/N 901-13, was found disconnected from the throttle and that the nut, bolt, washer, and cotter pin were missing.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# FTW95LA282