N1004W

Substantial
None

AIR TRACTOR AT-401 S/N: 401-0687

Accident Details

Date
Tuesday, July 11, 1995
NTSB Number
FTW95LA301
Location
CASH, AR
Event ID
20001207X03958
Coordinates
35.790817, -90.929389
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

ENGINE POWER LOSS DUE TO PARTIAL FAILURE OF ONE MAGNETO COMBINED WITH TOTAL FAILURE OF THE OTHER MAGNETO. A FACTOR WAS THE LACK OF SUITABLE TERRAIN FOR A FORCED LANDING.

Aircraft Information

Registration
N1004W
Make
AIR TRACTOR
Serial Number
401-0687
Year Built
1988
Model / ICAO
AT-401

Registered Owner (Historical)

Name
RIDDELL FLYING SERVICES INC
Address
PO BOX 2482
Status
Deregistered
City
WEST HELENA
State / Zip Code
AR 72390-0482
Country
United States

Analysis

On July 11, 1995, at 1140 central daylight time, an Air Tractor AT-401, N1004W, nosed over during a forced landing near Cash, Arkansas. The commercial pilot was not injured and the airplane sustained substantial damage. No flight plan was filed for the aerial application flight conducted by Morrison Aircraft Corporation under Title 14 CFR Part 137. Visual meteorological conditions prevailed for the flight which departed a private airstrip near Cash at 1135 CDT.

According to the pilot, he was en route to fertilize a field when the engine lost power and began "backfiring, missing and smoking." The pilot dumped the load of Urea and attempted to return to the private airstrip. The engine continued to lose power and the pilot landed in a soybean field. The airplane nosed over and came to rest inverted. Damage included a bent vertical stabilizer and rudder and deformed rear fuselage longerons.

The operator arranged to have a certified repair station examine the magnetos. When run on a test stand, one of the magnetos failed to spark. Disassembly revealed that an internal drive gear had failed. The other magneto was tested and failed to spark below 400 rpm and displayed "erratic misfiring" above 400 rpm. The point gap clearance was measured and found to be "too wide causing misfiring at low and high rpm."

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# FTW95LA301