N200CT

Substantial
None

MOONEY M-20-M S/N: 27-0016

Accident Details

Date
Thursday, July 13, 1995
NTSB Number
LAX95LA251
Location
SANTA MONICA, CA
Event ID
20001207X03999
Coordinates
34.009963, -118.459487
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

the pilot's improper remedial action during an aborted takeoff due to an improperly installed pitot line to the airspeed indicator.

Aircraft Information

Registration
Make
MOONEY
Serial Number
27-0016
Engine Type
Reciprocating
Year Built
1989
Model / ICAO
M-20-M M20P
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
M20M

Registered Owner (Current)

Name
ALPHA BRAVO 1 LLC
Address
7 BREEZY KNOLL RD
City
WILLOW STREET
State / Zip Code
PA 17584-9340
Country
United States

Analysis

QcOn July 13, 1995, at 0727 hours Pacific daylight time, a Mooney M-20-M, N200CT, was substantially damaged during an aborted takeoff at Santa Monica, California. The pilot and passenger were not injured. Visual meteorological conditions prevailed for the departure, and an instrument flight plan was filed. The flight was originating as a personal cross-country flight destined for Abilene, Texas.

The pilot stated that during the takeoff roll on runway 21, he realized that he had no airspeed indication. He chose to abort the takeoff at that point. At the west end of the runway, skid marks indicated that the airplane went sideways and the left landing gear collapsed. The left wing settled to the ground and fuel ignited from the wing fuel vent area. The brief fire burnt into the wing structure. The wing was also damaged from ground contact.

The pilot had contracted for repairs to the vacuum/instrument system while at Santa Monica. According to a Federal Aviation Administration (FAA) inspector, examination of the airspeed plumbing revealed that the plastic pitot tube was not connected at the airspeed indicator. Further examination of the tube failed to reveal a crush imprint from the "B" nut cone. The cone was found on the cockpit floor. An airspeed repair date of January 23, 1995, was affixed to the airspeed instrument case.

The pilot stated that the M20 brakes are not adequate to stop a TLS model, near gross weight, down hill with a slight tailwind. He stated that the brakes should have been enlarged with the gross weight increase. He further stated that he now has the double puck brakes and that they are much more effective.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX95LA251