N62PJ

Destroyed
Fatal

Fox Aircraft Corp. PEREGRINE PJ-2 S/N: 001

Accident Details

Date
Friday, August 4, 1995
NTSB Number
LAX95LA278
Location
MINDEN, NV
Event ID
20001207X04277
Coordinates
39.009574, -119.749420
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
1
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

a failure of the wing flap control system due to inadequate design, which led to an asymmetrical flap deployment during a critical flight condition and in-flight loss of control. A related factor was the lack of a split-flaps warning system.

Aircraft Information

Registration
N62PJ
Make
FOX AIRCRAFT CORP.
Serial Number
001
Engine Type
Reciprocating
Model / ICAO
PEREGRINE PJ-2 AT2P
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
FOX AIRCRAFT CORPORATION
Address
2207 BELLANCA ST
Status
Deregistered
City
MINDEN
State / Zip Code
NV 89423
Country
United States

Analysis

On August 4, 1995, at 0926 hours Pacific daylight time, a Fox Aircraft Corp., Peregrine PJ-2, N62PJ, collided with terrain after an in-flight loss of control during a go-around from runway 34 at the Douglas County Airport, Minden, Nevada. The airplane was being operated as a developmental test flight under 14 CFR Part 91 when the accident occurred. The airplane was destroyed. The commercial pilot was fatally injured. Visual meteorological conditions prevailed at the time.

The pilot reported a split flap situation by radio to his company during the go-around. Witnesses reported seeing the airplane turn left to the crosswind leg of the traffic pattern and then roll to the right. The airplane pitch attitude was observed decreasing and the airplane continued to roll until colliding with terrain.

Examination of the flap system revealed a pin sheared on the left-hand drive shaft. The flaps are driven by a single electric motor which rotates two independent flexible drive shafts that actuate the right and left flap panels. Examination of system drawings and descriptions revealed that a sheared pin would break the continuity of the respective flap panel drive, stopping the flap panel while the other flap panel would continue to extend or retract. There was no system or mechanism in the airplane that detected an asymmetrical flap condition.

The pin was submitted to metallurgical lab for analysis. According to the metallurgist, the pin conformed to the material specifications of the pin manufacturer and had failed due to overload shear forces on an approximate 45-degree plane. The metallurgist indicated the orientation of the direction of shear would indicate that a combination of torsional and axial loads were being applied at the time of the shear failure.

The airplane manufacturer conducted tests of the flap system. The manufacturer determined the electrical motor in the flap system was capable of shearing the pin before a circuit breaker would interrupt electrical power to the flap motor.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX95LA278