N4918G

Substantial
Minor

CESSNA 172N S/N: 17272465

Accident Details

Date
Saturday, September 9, 1995
NTSB Number
FTW95LA386
Location
KERRVILLE, TX
Event ID
20001207X04499
Coordinates
30.039716, -99.130004
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
4
Uninjured
0
Total Aboard
4

Probable Cause and Findings

the pilot's inadequate preflight preparation and his failure to use all the available runway. A factor was the dark night.

Aircraft Information

Registration
N4918G
Make
CESSNA
Serial Number
17272465
Engine Type
Reciprocating
Year Built
1979
Model / ICAO
172N C172
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
NEENWA ENTERPRISES INC
Address
1831 LAUREN PL
Status
Deregistered
City
MISSOURI CITY
State / Zip Code
TX 77489-3040
Country
United States

Analysis

On September 8, 1995, at 2300 central daylight time, a Cessna 172N, N4918G, was substantially damaged during an aborted takeoff at Kerrville Municipal/Louis Schreiner Field, Kerrville, Texas. The commercial pilot and three passengers sustained minor injuries. The airplane was being operated as a personal night cross country flight under Title 14 CFR Part 91. The flight originated in San Antonio, Texas at 2200. Visual meteorological conditions prevailed, and no flight plan was filed.

The pilot reported in a written statement that, after taxiing to runway 20, he did a runup, then "taxied onto the runway and gave full throttle." After realizing he was "running out of runway," he aborted the takeoff. He further reported that, after the incident, "I noticed that I had taxied onto the short runway."

The pilot reported to a Federal Aviation Administration (FAA) inspector that he taxied from the ramp, which is located near the helipad, to runway 20 via the taxiway that crosses near the midpoint of the runway. He further reported that, instead of turning right onto runway 20 and back taxiing to the end of the runway, he turned left and attempted to takeoff using approximately "1,300 feet" of runway.

Examination of the accident site by the FAA inspector revealed evidence of braking where the airplane crossed runway 12/30. See airport diagram. The airplane came to rest in a ditch approximately 150 feet beyond the runway. The left wing was buckled near the fuel tank and the engine was displaced to the right.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# FTW95LA386