N42RA

Substantial
Minor

Pro-built Aviation KITFOX IV SPEEDSTER S/N: GBS 036

Accident Details

Date
Saturday, September 30, 1995
NTSB Number
LAX95LA345
Location
LAKEPORT, CA
Event ID
20001207X04533
Coordinates
39.039047, -122.929168
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
2
Uninjured
0
Total Aboard
2

Probable Cause and Findings

the pilot's improper installation of the carburetors.

Aircraft Information

Registration
N42RA
Make
PRO-BUILT AVIATION
Serial Number
GBS 036
Engine Type
None
Year Built
1994
Model / ICAO
KITFOX IV SPEEDSTER FK9
No. of Engines
0

Registered Owner (Historical)

Name
PRO BUILT AVIATION INC
Address
PO BOX 2403
Status
Deregistered
City
MARTINEZ
State / Zip Code
CA 94553
Country
United States

Analysis

On September 29, 1995, at 1747 hours Pacific daylight time, an experimental Pro-Built Aviation, Inc., Kitfox IV Speedster, N42RA, crashed after experiencing a loss of engine power shortly after departing runway 28 at Lampson Airport, Lakeport, California. The pilot was beginning a local visual flight rules personal flight. The airplane, registered to Pro-Built Aviation, Inc., Martinez, California, sustained substantial damage. The certificated private pilot and passenger received minor injuries. Visual meteorological conditions prevailed.

The pilot told National Transportation Safety Board investigators in a telephone interview conducted on September 29, 1995, that the engine began to run rough shortly after reaching 300 feet above the ground. The pilot applied the fuel boost pump to alleviate the roughness, but without success.

When it became evident that a forced landing was inevitable, the pilot elected to land in an open area. As he approached the open area, the pilot realized that the airplane's altitude was insufficient to clear a corral and high tension wires. He then intentionally stalled the airplane about 8 feet above the ground to avoid hitting the obstacles and landed in an 80-foot-long open area.

On December 8, 1995, an FAA airworthiness inspector from the Sacramento [California] Flight Standards District Office, a representative from A.C. Ultra Aviation (the engine manufacturer), and an independent fixed-base operator disassembled the engine for examination.

According to the FAA inspector, the engine was intact and sustained minor impact damage. He said that he found unidentified material near the flywheel and the magnets. The distributor coil was free of the material.

Investigators established continuity of the engine gear and valve train assembly.

The left carburetor throttle slide valve was found installed 90 degrees off its proper position; the right throttle slide valve was installed according to the manufacturer's maintenance manual. Fuel stains were found on the left carburetor valve.

The right carburetor choke arm nut was missing and the choke was partially open. The carburetor vent lines were extended and did not comply with the manufacturer's installation recommendations. The ignition system produced sparks when the engine was rotated with the starter.

The manufacturer's representative said that the left-hand carburetor slide valve and right carburetor activated choke would result in "excessive vibration, engine stumbling, and possible stoppage." He also said that "the incorrectly routed fuel vent lines would create a differential pressure between the carburetor intakes and float bowl chambers, which also would create unstable fuel delivery, rough running, excessive vibration, and possible stoppage."

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX95LA345