N693MA

Substantial
None

PIPER PA-31 S/N: 31-7852005

Accident Details

Date
Thursday, October 19, 1995
NTSB Number
CHI96LA014
Location
ANDERSON, IN
Event ID
20001207X04668
Coordinates
40.130168, -85.760772
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
3
Total Aboard
3

Probable Cause and Findings

inadequate maintenance in that an engine oil line was not properly tightened after routine maintenance. A factor was the disconnected oil line.

Aircraft Information

Registration
N693MA
Make
PIPER
Serial Number
31-7852005
Engine Type
Reciprocating
Model / ICAO
PA-31 PA31
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Analysis

On October 19, 1995, at 0547 eastern standard time (est), a Piper PA-31, N693MA, piloted by a commercial pilot was substantially damaged from a left engine fire in cruise flight. Visual meteorological conditions prevailed at the time of the accident. The personal 14 CFR Part 91 flight was operating on a IFR flight plan. The pilot and two passengers reported no injuries. The flight departed from Munice, Indiana, at 0530 edt.

The pilot stated that he had just leveled off the aircraft at 4000 feet mean sea level. Shortly thereafter, the left engine area erupted in flames. Upon seeing the fire the pilot pulled the mixture control to idle cutoff, and shut off the fuel selector valve for the left engine. However, the fire continued in the engine area until landing. The pilot received a vector from Indianapolis Approach Control for the emergency descent/landing at Anderson, Indiana. A post flight examination by the Federal Aviation Administration revealed that the left engine's turbocharger oil line was not attached at the accessory case on the engine.

In a telephone interview with the pilot he stated that during the preflight he checked the oil on both engines, but did not open the engine side inspection doors. The pilot stated he did not feather the left engine, because he needed the extra drag to execute the rapid descent. The windmilling prop would drive the engine's oil pump, causing the engine's oil to be expelled out the accessory case opening.

A telephone interview was conducted with the director of maintenance (DOM) for the company that owned N693MA. He stated this was the aircraft's first flight after a 50 hour inspection. The DOM said that a different mechanic had worked on each engine. The inspection was accomplished in accordance with Piper service report #230764. N693MA was then run up and checked for oil leaks, with none found. The DOM stated that it was not normal practice to remove the oil line to the turbocharger during a 50 hour inspection.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI96LA014