N84124

Substantial
Minor

AERONCA 7AC S/N: 7AC-2811

Accident Details

Date
Sunday, October 29, 1995
NTSB Number
CHI96LA023
Location
LAPEER, MI
Event ID
20001207X04676
Coordinates
43.040515, -83.319427
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
2
Uninjured
0
Total Aboard
2

Probable Cause and Findings

fuel exhaustion resulting in engine failure, the inadvertant stall, and improper decision by the pilot to attempt a large heading change at low altitude and airspeed. A factor relating to this accident is no fuel quantity gage installed in the airplane.

Aircraft Information

Registration
Make
AERONCA
Serial Number
7AC-2811
Engine Type
Reciprocating
Model / ICAO
7AC CH7A
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
7AC

Registered Owner (Current)

Name
MUSSMAN CRAIG
Address
10250 N 16000E RD
City
GRANT PARK
State / Zip Code
IL 60940-5151
Country
United States

Analysis

On October 29, 1995, at 1730 eastern standard time (est), an Aeronca 7AC, N84124, piloted by a private pilot, sustained substantial damage when after takeoff from a touch and go landing the airplane's engine quit. The airplane subsequently impacted the terrain after the pilot attempted to land on the opposite runway. Visual meteorological conditions prevailed at the time of the accident. The flight was operated under 14 CFR Part 91. A flight plan was not on file. The pilot reported minor injuries to himself and his passenger. The airplane was on a local flight which took off from Lapeer, Michigan, at 1200 est.

In his written statement, the pilot reported the airplane had climbed to about 500 feet above ground level after takeoff on runway 27 when the engine lost power. He determined that he had enough altitude to turn the airplane around and land on the opposite runway. "There was a west wind of about 10 miles an hour." When the airplane crossed the approach end of runway 09 "the engine started running again." The pilot stated that the airplanes's nose down attitude must have allowed what remaining fuel he had in the system to reach the engine. Before the pilot could close the throttle, "the airplane ballooned into the air." With the tailwind and extra altitude, the pilot determined that he would not be able to land the airplane without running off the end of the runway. He then decided to attempt a landing on runway 32, the airport's diagonal runway. This maneuver required the pilot to execute a left 130 degree heading change at low altitude and airspeed. Concerned with a tree line ahead of him which ran parallel to runway 32, the pilot tightened his turn. At approximately 10 to 20 feet above ground level, the airplane "stalled," impacted the terrain left wing first and came to rest on runway 32.

The pilot also reported in his written statement that the airplane had two gallons of fuel on board at the last takeoff.

The Federal Aviation Administration (FAA) inspector who examined the wreckage found no evidence of fuel at the accident site. Examination of the airplane's fuel system showed no indications of fuel in the carburetor, fuel lines or tank prior to impact. The airplane did not have a fuel quantity gage installed.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI96LA023