N9205F

Substantial
Minor

HUGHES 369HS S/N: 440583S

Accident Details

Date
Thursday, October 12, 1995
NTSB Number
LAX96LA009
Location
HANA, HI
Event ID
20001207X04722
Coordinates
20.770824, -155.989379
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
4
Uninjured
1
Total Aboard
5

Probable Cause and Findings

the loss of engine power due to inadequate maintenance inspection of the fuel system which permitted air to enter the engine fuel supply. A factor in the accident was the pilot's improper execution of the autorotation landing.

Aircraft Information

Registration
N9205F
Make
HUGHES
Serial Number
440583S
Year Built
1974
Model / ICAO
369HS

Registered Owner (Historical)

Name
ALEXANDER STEVEN H
Address
355 HUKILIKE STREET SUITE 211
Status
Deregistered
City
KAHULUI
State / Zip Code
HI 96732
Country
United States

Analysis

On October 11, 1995, at 1755 hours Hawaiian standard time, a Hughes 369HS, N9205F, was substantially damaged during an emergency landing shortly after takeoff from Hana Airport on the island of Maui, Hawaii. The commercial pilot was not injured, however, his four passengers received minor injuries. The aircraft was being operated as a sightseeing flight by AlexAir under 14 CFR Part 135 when the accident occurred. Visual meteorological conditions prevailed and a company VFR flight plan was filed.

The pilot reported departing from runway 8/26 at midfield. Upon reaching 100 feet altitude at 60 knots, he experienced a lateral vibration he thought was due to rotor imbalance. He had lowered the collective control and slowed for a normal descent when he noted that the fuel filter light had come on. This was followed immediately by the engine failure light and warning horn, and a loss of engine power. The pilot said he then initiated an autorotation back to the runway. He "lowered collective and nosed the helicopter forward to try to get some airspeed for a flare at about 30 feet," however, he was unable to flare and level the helicopter before the tail boom and landing skids impacted at the same time on the runway. The main rotor blades then flexed downward and severed the tailboom.

Subsequent examination of the aircraft by inspectors from the FAA's Honolulu Flight Standards District Office revealed that there was a leak in the fuel filter bypass switch which allowed air to enter the suction-fed engine fuel system. The fuel filter bypass switch was manufactured by the R. W. Jenson Company as part number 800175-3 (McDonnell Douglas Helicopter/Hughes P/N 369H8144) circa 1974. The last 100-hour inspection of the aircraft was performed 77 hours prior to the accident.

Following the accident the switch was inspected and tested at Spectra-Lux Corporation, who currently manufacture the switch under license. The inspection revealed leakage between the mating flange halves. The leakage was due to deteriorated safety wiring which permitted the machine screws holding the flanges together to loosen. When the screws were tightened, the leakage stopped and the switch functioned to the manufacturers' specifications.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX96LA009