N912XL

Substantial
Fatal

LOUKS PULSAR XP S/N: 251

Accident Details

Date
Saturday, October 7, 1995
NTSB Number
MIA96LA004
Location
INVERNESS, FL
Event ID
20001207X04752
Coordinates
28.830974, -82.270637
Aircraft Damage
Substantial
Highest Injury
Fatal
Fatalities
1
Serious Injuries
1
Minor Injuries
0
Uninjured
0
Total Aboard
2

Probable Cause and Findings

Premature rotation by the pilot during takeoff, which resulted in an inadvertent stall/mush, while attempting to accelerate in ground effect after lift-off.

Aircraft Information

Registration
N912XL
Make
LOUKS
Serial Number
251
Engine Type
Reciprocating
Year Built
1993
Model / ICAO
PULSAR XP SA02
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
LOUKS RAYMOND L
Address
352 CARTER RD
Status
Deregistered
City
DEFIANCE
State / Zip Code
OH 43512
Country
United States

Analysis

On October 7, 1995, about 1352 eastern daylight time, a homebuilt Pulsar XP, N912XL, crashed during takeoff from the Inverness Airport, Inverness, Florida. Visual meteorological conditions prevailed at the time and no flight plan was filed for the 14 CFR Part 91 personal flight. The airplane was substantially damaged by impact and a postcrash fire and the commercial-rated pilot sustained serious injuries. One passenger who was seriously injured died 13 days after the accident. The flight was originating at the time of the accident.

The pilot stated that he performed an engine run-up before takeoff with no discrepancies noted. During the takeoff ground roll under no wind condition with the flaps retracted, he intentionally remained on the ground for a longer time. After rotation he lowered the nose of the airplane to accelerate during which the airplane rolled to the left, descended, and touched down. While on the ground travelling about 10-15 miles per hour, the right wing of the airplane collided with a runway marker sign. The airplane then spun to the right and came to rest on a heading of about 085 degrees. A postcrash fire started on the right side of the airplane after it came to rest. He reported that he rescued his wife who was uninjured as a result of the collision with the sign, out the left side of the airplane. He further stated that there was no preimpact failure or malfunction of the engine or flight controls.

A witness who was located about 150 yards south of the airport observed the airplane during the takeoff ground roll and stated that it appeared to him that the airplane was in a nose high attitude. The airplane climbed to 6-7 feet above the runway then was observed to roll to his right and disappeared behind trees.

Information pertaining to the weather is contained in an NTSB Weather Factual Report. The pilot later reported that the wind condition was calm at the time of the accident.

According to the designer of the airplane, the calculated stall speed at the time of the accident was about 48 miles per hour.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# MIA96LA004