N27RV

Destroyed
Fatal

CHARD RV-3A S/N: 27A1

Accident Details

Date
Sunday, October 8, 1995
NTSB Number
SEA96LA005
Location
FOREST GROVE, OR
Event ID
20001207X04790
Coordinates
45.549171, -123.149024
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
1
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

The pilot exceeded the design stress limit of the aircraft, followed by the failure of the right wing main spar.

Aircraft Information

Registration
N27RV
Make
CHARD
Serial Number
27A1
Engine Type
Reciprocating
Model / ICAO
RV-3A RV3
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
MOSELEY HUGH STEPHENS
Address
9870 NW GORDON RD
Status
Deregistered
City
CORNELIUS
State / Zip Code
OR 97113
Country
United States

Analysis

On October 8, 1995, approximately 1640 Pacific daylight time, an experimental Chard RV-3A, N27RV, experienced an inflight separation of the right wing. The commercial pilot, who was the sole occupant, received fatal injuries, and the aircraft was destroyed. The personal pleasure flight, which departed Sunset Airpark about 40 minutes earlier, was being operated in visual meteorological conditions at the time of the accident. No flight plan had been filed, and there was no report of an ELT activation.

According to witnesses, the RV-3 followed an RV-8 in a steep climbing maneuver, and then initiated a level steeply banked turn. During this turn, which was described by witnesses on the ground as an extremely tight right turn, the right wing of the RV-3 was seen to depart the fuselage. The fuselage and remaining wing descended to the ground, impacting in an inverted position.

According to Van's Aircraft Change Notice CN-1, Van's Aircraft performed stress analysis calculations prior to releasing the RV- 3 plans, and the calculations determined that the major wing components should withstand loads of 9 G's before failure. In addition, Van's Aircraft performed a static load test on an RV-3 structure, which was built according to plans, and the main wing spar failed at 9 g's. The recording accelerometer found in the wreckage of N27RV was indicating a positive 9.2 G's.

Examination of the wreckage revealed that the forward wing spar had failed just outboard of the attach fitting, and the rear spar, and rear spar root doubler plate, had fractured through the spar-to-fuselage attach bolt hole.

The rear spar root and rear spar root doubler were sent to the NTSB Materials Laboratory for a metallurgical examination. The examination of both pieces revealed features and deformation patterns consistent with overstress separation. No evidence of fatigue failure was found.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# SEA96LA005