N88TK

Destroyed
Minor

BITONTI WITTMAN WT-8 S/N: MSB-1

Accident Details

Date
Saturday, December 16, 1995
NTSB Number
CHI96LA054
Location
PLYMOUTH, MI
Event ID
20001207X04976
Coordinates
42.369934, -83.460792
Aircraft Damage
Destroyed
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
0
Total Aboard
1

Probable Cause and Findings

a stuck exhaust valve resulting in an overtemperature condition of the cylinder, the pilot's continued operation without corrective maintenance, and his failure to maintain aircraft control.

Aircraft Information

Registration
N88TK
Make
BITONTI
Serial Number
MSB-1
Year Built
1993
Model / ICAO
WITTMAN WT-8

Registered Owner (Historical)

Name
BITONTI FRANK E
Address
8337 ESPER
Status
Deregistered
City
DETROIT
State / Zip Code
MI 48204
Country
United States

Analysis

On December 16, 1995, at 1038 eastern standard time (est), a Bitonti-Wittman WT-8, N88TK, was destroyed during a collision with the ground shortly after takeoff from Canton-Plymouth Mettetal Airport, Plymouth, Michigan. The private pilot reported minor injuries. The personal 14 CFR Part 91 flight was operating in visual meteorological conditions. No flight plan was on filed.

According to the pilot's written statement, he said when he started the engine that morning he had a hard time keeping the engine running below 1100 RPM. After takeoff at about 300 feet, the pilot observed the engine's cylinder head temperature had reached the red zone, so he pulled back on the throttle. When he pulled back slightly on the throttle, total power loss occurred. The pilot maneuvered the airplane to avoid houses and noticed a small clearing in a storage lot so he decided to land there. On descent, the pilot lost control of the airplane and the right wing struck two trailers and two boats. The airplane was consumed by post crash fire. The pilot was found sitting under the left wing and was pulled to safety.

A Federal Aviation Administration Principal Maintenance Inspector (PMI), represented the NTSB on-scene. The PMI said the engine examination revealed that the #1 cylinder had no compression because of a stuck open exhaust valve and the compression in cylinder #3 was weak. The exhaust valve springs were very weak. The pilot told the PMI that in the past he has had hot cylinder head temperatures before and that pulling back on the throttle had worked previously.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI96LA054