Accident Details
Probable Cause and Findings
failure of the copilot (pilot-rated cargo loader, who was flying the aircraft) to establish and maintain a positive rate of climb after taking off at night; and inadequate supervision by the pilot-in-command (PIC), by failing to ensure that proper altitude was obtained and maintained during the departure. Factors relating to the accident were: darkness; the lack of visual cues; and the resultant visual illusion, which the copilot failed to recognize during the night departure. Also, the lack of a restraint system (seat belt and/or shoulder harness) for the passenger was a possible related factor.
Aircraft Information
Registered Owner (Historical)
Analysis
HISTORY OF FLIGHT
On January 29, 1996, at 0435 hours Hawaiian standard time, a Cessna 402B, N999CR, collided with gradually rising terrain while on takeoff from the Wiamea-Kohala Airport, Kamuela, Hawaii. The aircraft was destroyed. The certificated airline transport pilot sustained fatal injuries, and two onboard cargo loaders received serious injuries. The aircraft was being operated as a contract mail flight by Trans Executive Airlines of Hawaii under 14 CFR Part 135 when the accident occurred. The flight originated in Honolulu, Hawaii, at 0200. The flight departed Kamuela on the return leg of the flight at 0430. Visual meteorological conditions prevailed at the time and no flight plan had been filed.
A worker at the Waimea-Kohala airport reported that about 0530 on the morning of the accident he heard a knock on his door. When he opened the door he saw one of the cargo loaders (hereafter referred to as cargo loader No. 2) who told him that he had just been involved in an aircraft accident. The cargo loader told the worker that he heard a sound he did not recognize and the next thing he remembered was being outside the aircraft. He looked around, saw the airport beacon, and began walking toward it. He estimated that it took him between 45 minutes to 1 hour to reach the airport, which involved climbing over two fences.
One of the police officers who first responded to the scene told the Safety Board that the night was very dark with a clear sky and calm winds. From his vantage point at the accident site, he was unable to see any ground lights toward the south or east.
On the date of the accident police officers interviewed cargo loader No. 2, who had been in the cargo compartment. During the interview, he reportedly told officers that when they left Waimea his friend (cargo loader No. 1) was flying the aircraft, while the pilot acted as the copilot. He later told FAA inspectors who spoke with him on April 24, 1996, that he did not recall who was flying the aircraft. (The Hawaii Police Department report is appended to the report.)
After several attempts by the Safety Board and the Honolulu FSDO to contact cargo loader No. 1, on April 23, 1996, he responded to the FSDO inspector by letter, in which he admitted performing copilot duties, but denied flying the aircraft. According to FAA inspectors, he stated that he remembered something abnormal happened with one of the engines because it was sputtering. He said he looked at the engine gauges and they were not right.
PERSONNEL INFORMATION
The operator reported the pilot-in-command for the Part 135 flight was current and qualified in the aircraft with about 1,250 hours in the Cessna 402. He had previously flown this regularly scheduled mail flight to and from the airport. The operator stated that the pilot was not authorized to carry company personnel or passengers without required seating. He was, however, permitted to allow rated employees to fly the aircraft on Part 91 positioning and ferry segments. He explained that he did not pay the cargo loaders, but rather allowed them to build multiengine flight time on these flights as compensation.
Cargo loader No. 1 held a commercial pilot certificate, with multiengine and instrument ratings. A pilot's logbook found in the aircraft wreckage bore his name. A review of that logbook revealed that he had logged pilot-in-command time on 47 company flights from December 23, 1995, through January 22, 1996. The logbook also showed that 23 of those flights were flown over the same route as was being flown at the time of the accident.
AIRCRAFT INFORMATION
A review of the aircraft, engine, and propeller logbooks was conducted by the Safety Board, FAA airworthiness inspectors, and manufacturers' representatives. No discrepancies related to airworthiness were identified. (Extracts of aircraft maintenance records are appended to this report.)
The aircraft had been manufactured and delivered with auxiliary and winglocker fuel tanks in addition to the main fuel tip tanks. However, both the auxiliary and winglocker fuel tanks had been removed from the aircraft, resulting in a total fuel capacity of 102 gallons.
The aircraft was configured for an all cargo flight with seating limited to the pilot and copilot.
WRECKAGE AND IMPACT INFORMATION
The aircraft crashed on open rolling terrain about .3 miles south of runway 04 at 19 degrees 59.55 minutes north latitude and 155 degrees 39.55 minutes west longitude. The first evidence of ground contact was east, abeam the departure end of runway 04. At this location, ground scars and debris identified as components from the right wing, were near a protruding 5-foot rock formation. The rock formation exhibited an impact mark about 1 foot from its top, which, at that point, was about 2,686 feet msl. The debris included portions of the right tip tank, including the fuel boost pump and the right outboard aileron hinge bracket. The initial ground scar and debris path were along a 148-degree bearing.
There was no evidence of subsequent ground contact for about 128 feet until a second ground scar was located. Sixteen perpendicular slash marks were noted along this scar, and measured on average about 24.25 inches apart. The second ground scar was along a 160-degree bearing.
The final ground scars were about .5 miles south of the airport and .7 miles from the initial impact point along a 264-degree bearing. The terrain at this point had risen to an elevation of about 2,711 feet msl. These ground scars were located on the ascending side of a grassy knoll. The initial portion of the scar revealed five additional perpendicular slashes, averaging about 26 inches between slashes. During the impact sequence the left engine and propeller separated from the left wing. The aircraft continued up and over its crest for an additional 207 feet. The aircraft came to rest on a 072-degree bearing. The relative bearing between the second and final ground scars was 218 degrees.
A ground speed was computed for the first three propeller slashes in the first series of 17 marks using 2,450 rpm. A similar computation was made for the first three propeller slashes in the last series of five marks also using 2,450 rpm. (The theoretical formula and the actual computations are appended to this report.)
An on-site examination was conducted by the Safety Board investigator in coordination with an FAA airworthiness inspector. The aircraft was later re-examined by representatives from the aircraft and engine manufacturers under the supervision of an FAA airworthiness inspector.
All flight control surfaces and load bearing structures were located between the initial point of impact and the final position of the aircraft. Control continuity was not established due to the extent of damage to the airframe, flight control surfaces, and the numerous breaks in the control cables, rods, cranks, and pulleys. No evidence was found of preimpact control binding or chaffing associated with any of the control linkages.
There was an approximate 90 percent empennage separation near FS 213. The nose section of the aircraft was crushed aft to about FS 167. Both wings exhibited leading edge damage as well as buckling, bending, and structural separation. There was impact damage on the top of the vertical stabilizer along with an aft and downward collapse of the forward cabin area. The horizontal stabilizer and elevators exhibited impact damage and were found separated from the empennage.
The landing gear was found in the up and locked position while the wing flaps were in the full up position. The flap motor showed five links extending from the top of the chain drive sprocket to a point where the chain transitions to a cable. The flap control handle and indicator also indicated less than the flaps full up position. The aircraft representative was able to quantify the preimpact trim position of the rudder as neutral and the aileron trim as 0 degrees, with the tab neutral. The flap position and elevator trim setting were considered unreliable due to structural damage, control separation, and possible movement during the impact sequence.
Both main fuel tip tanks were destroyed during the impact sequence. The forward bulkhead of the right tank had ruptured and was separated from the tank. The left main tip tank was also separated and exhibited evidence of distortion. The fuel valves for both tanks were found in the "open" position. The fuel sector switch for the left tank was found on "main" while the switch for the right tank had been destroyed.
Both engines separated from their mounts and both propellers separated from their respective crank flanges. Both engines were examined by the engine manufacturer under the direct supervision of an FAA airworthiness inspector. Valve train continuity was established to the accessory section through the hand rotation of the crank flange and observing the rotation at the aft end. Hand rotation established thumb compression in all six cylinders of both engines. The right vacuum pump was removed and hand rotated, establishing the pump's mechanical continuity. Both engine fuel pumps were removed, examined, and found to be mechanically intact. The engine fuel screens were removed and examined. Both fuel control units' fuel screens were also examined. The left engine fuel manifold was disassembled and that screen examined. There was no evidence of foreign substances found on any of the screens.
As each engine was hand rotated, a spark was obtained from at least one of the magnetos. The top spark plugs were removed from both engines and examined. There was no evidence of oil, carbon, or lead fouling on any plug. According to the Champion check-a-plug chart, there was no unserviceable erosion on any of the plugs' massive electrodes.
Both propellers were recovered and examined. The left propeller was found on the feather stop whil...
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX96FA103