Accident Details
Probable Cause and Findings
The pilot's failure to maintain a proper altitude, and insufficient obstruction lighting requirements established by the Federal Aviation Administration and the Federal Communications Commission.
Aircraft Information
Registered Owner (Historical)
Analysis
HISTORY OF FLIGHT
On February 9, 1996, at 2051 eastern standard time, a Cessna P206A, N4655F, was. destroyed during a collision with a tower near Forks Township, Pennsylvania. The airline transport pilot was fatally injured. Night visual meteorological conditions prevailed for the personal flight that originated at Pittstown, New Jersey, about 2040. No flight plan had been filed for the flight conducted under 14 CFR Part 91.
According to witnesses, the pilot purchased the airplane in November, 1995, and based it at the Easton Airport (N43), Easton, Pennsylvania. On February 9, 1996, he flew N4655F from N43 to the Sky Manor Airport (N40), Pittstown, New Jersey, and topped off the fuel tanks. The pilot returned to N43, about 1730, and again flew back to Sky Manor. The pilot had dinner at N40, and then departed on the last leg for Easton.
In a police report that contained summaries of witness interviews, a witness 1/2 of a mile southeast of the accident stated:
"...he saw the aircraft gliding down. [He] heard a buzzing noise, but he is not sure if the aircraft engine was running. [He] said the aircraft was low as though it were going down...Aircraft was traveling parallel to McCartney St. and veered left. Approximately 10 seconds after seeing the aircraft, [he] heard what he thought was a gunshot."
Three witnesses near the accident scene stated that they were about to inform a radio station that their tower obstruction lights were not on, when they observed an airplane collide with the tower. One of the witnesses stated that he heard the airplane's engine running when the collision occurred.
The accident occurred during the hours of darkness about 40 degrees, 43 minutes north latitude, and 75 degrees, 13 minutes west longitude.
PERSONNEL INFORMATION
The pilot, Mr. Donald C. Cory, held an Airline Transport Pilot Certificate with a rating for airplane multiengine land, and a Commercial Pilot Certificate with a rating for airplane single engine land. He also held a Flight Instructor Certificate for airplane single engine land and instrument airplane.
His most recent Federal Aviation Administration (FAA) First Class Medical Certificate was issued on January 11, 1996.
Mr. Cory's pilot log book was located; however, it did not contain any flight hours from his employment with the airlines. Mr. Cory's total flight time was estimated to be about 24,500 hours, of which approximately 3,500 hours were in single engine airplanes. He had accumulated about 30 hours flying experience in this make and model.
OTHER DAMAGE
The airplane struck a tower owned and operated by WEEX, Inc., Easton, Pennsylvania. The tower held antennas for the commercially licensed WIPI, AM, and WODE, FM, radio stations. The top of the tower was 928 feet above mean sea level (MSL). A 10 foot section of the top of the tower was bent over on a magnetic bearing of approximately 315 degrees.
COMMUNICATIONS
There was no record of the pilot receiving a weather briefing, notices to airmen, or filing a flight plan.
AERODROME INFORMATION
The Easton Airport was located about 2 miles northwest of the 928 foot antenna. The airport field elevation was 399 feet MSL, and the recommended traffic pattern altitude was 1,400 feet MSL. Runway 36/18 was the only lighted runway, and there was no visual glideslope indicator available for runway 36.
WRECKAGE AND IMPACT INFORMATION
The airplane wreckage was examined at the accident site on February 10, 1996, and revealed that all major components of the airplane were accounted for at the scene. The airplane came to rest nose down at a ground elevation of about 400 feet MSL, about 650 feet north of the tower.
The right wing was separated from the fuselage, and located about 250 feet east of the tower in the center of a road. The inboard leading edge of the wing contained orange paint marks, similar to the orange paint found on the top of the tower. Several pieces of the right wing, horizontal stabilizer, and the right main landing gear were scattered around the base of the tower. A 5-inch-diameter tree branch at the wreckage site displayed an area with a smooth cut. The cut was at an approximate 60 degree angle to the length of the branch.
Aileron control cable ends remained attached to the ailerons. The broken ends of the cables extended from the wings where they were separated from the fuselage. Further control continuity was not confirmed due to impact damage. Examination of the flap handle and actuators indicated that the flaps were retracted.
The engine and propeller remained attached to the fuselage, and were removed to a hanger for further examination. The propeller hub and blades were attached to the engine. Two of the three propeller blades displayed chord wise twisting and scratches. The tips of the blades displayed similar twisting, curling, wrinkling, and gouges.
Examination of the engine revealed the left and right magneto flanges received impact damage, and the magnetos were separated from the accessory case. The magnetos remained attached to the spark plug leads, and when the magnetos were rotated by hand, spark was observed at the end of the leads.
The engine fuel pump shaft was not sheared and rotated freely in the pump. The fuel control screen was opened and contained some debris and fuel; however, the screen was not clogged. The fuel manifold was absent of debris and fuel.
The propeller hub and blades were rotated and the engine crankshaft rotated freely. Valve train continuity was confirmed on all cylinders. Compression was determined on all cylinders by the thumb method, except the number five cylinder. The oil cooler was observed to be compressed into the number five cylinder barrel, and the valve cover was broken free of the cylinder. All spark plugs were absent of debris, and were light gray in color.
MEDICAL AND PATHOLOGICAL INFORMATION
An autopsy was performed on Mr. Donald C. Cory, on February 10, 1996, by Dr. Isiadore Mihalakis, of the North Hampton County Coroner's Office, Easton, Pennsylvania.
Toxicological testing was conducted by the FAA Toxicology Accident Research Laboratory, Oklahoma City, Oklahoma, and the North Hampton County Coroner's Office, Easton, Pennsylvania.
The toxicological testing report from the North Hampton County Coroner's Office was positive for 0.03 percent ethanol in the blood, and in 0.06 percent ethanol in the gastric.
According to 14 CFR Part 91, which addressed the use of alcohol and drugs, it stated, "No person may act or attempt to act as a crewmember of a civil aircraft...While having a .04 percent by weight or more alcohol in the blood..."
ADDITIONAL INFORMATION
The top of the 928 foot tower was about 2 miles south, and 1/2 mile east, of Easton's runway 36 center line. The top of the tower was 428 feet above ground level (AGL), and was located on the north, down slope side of a hill, at approximately 500 feet above mean sea level (MSL). The hill top south of the tower was about 575 feet MSL. A tower about 150 feet AGL was positioned about 100 feet north of the 928 foot tower. The 928 foot tower was equipped with lighting as specified by the Federal Communication Commission Rules. The 150 foot tower was not lighted.
A review of the engineering data for the 928 foot tower revealed that the actual height of the tower, with the obstruction lighting installed, was 930.5 feet MSL.
The 928 foot tower obstruction lights were reported out of service by the radio station on January 24, 1996, about 1955, to the Williamsport Flight Service Station. Williamsport issued a notice to airmen (NOTAM), about 2040, regarding the lighting outage. The NOTAM was valid until February 9, 1996. On February 8, 1996, at the request of the radio station, the NOTAM was reissued, valid until February 24.
During an interview with the radio station's engineer, he stated that he expected the lights to be inoperative for at least 6 weeks, and no temporary repairs were initiated by the radio station. He stated that the Austin Ring lighting transformer that was inoperative had to be custom made.
An engineering firm in the Allentown area was consulted by the NTSB Investigator about temporary repairs. The engineering firm representative stated that a "lighting choke" could have been used as a temporary repair, and could have had the lights operating within 24 hours. The cost of the repair was estimated at less than $500.
A third tower was situated along the same hill, about 2,100 feet east of the 928 foot tower. The top of the third tower was about 775 feet MSL. The top of the tower was illuminated by a single flashing red light, as specified by the Federal Communications Commission Rules.
The New York Sectional Aeronautical Chart depicted the location of the accident tower by the symbol for "group obstruction." Next to the symbol was the number "928," which according to the map legend, represented "elevation of the top above mean sea level." The symbol did not depict the number of towers that it represented, the individual tower heights, the proximity of the towers, or lighting.
A review of the New York Sectional revealed that the 16 mile direct route between Sky Manor and Easton, crossed directly over the group obstruction marking on the sectional. During the accident flight, only the 775 foot tower was illuminated.
A plot of the direct route between Sky Manor and Easton, and the actual route flown, revealed that the airplane flew east of the direct route between the two airports. A review of an Easton road map revealed that the co-owner of the airplane resided about 900 feet east of the actual route flown.
Obstruction Lighting and Marking
According to 14 CFR Part 77, the FAA was charged with the responsibility to identify obstructions to air navigation,. The c...
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# NYC96FA061