N3295C

Substantial
None

Beech E35 S/N: D-3962

Accident Details

Date
Sunday, April 14, 1996
NTSB Number
FTW96LA169
Location
ALBUQUERQUE, NM
Event ID
20001208X05557
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

a partial loss of engine power for undetermined reasons, and the pilot's failure to abort the takeoff.

Aircraft Information

Registration
N3295C
Make
BEECH
Serial Number
D-3962
Engine Type
Reciprocating
Model / ICAO
E35 BE35
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
NELSON ROGER
Address
675 N AERO DR HNGR 1
Status
Deregistered
City
CASA GRANDE
State / Zip Code
AZ 85222-8215
Country
United States

Analysis

On April 14, 1996, at 1410 mountain daylight time, a Beech E35, N3295C, was substantially damaged during a forced landing following an engine power loss on takeoff near Albuquerque, New Mexico. The airplane was registered to, and operated by, a private owner under Title 14 CFR Part 91. The private pilot and the passenger were not injured. Visual meteorological conditions prevailed and a flight plan was not filed. The local personal flight was originating from the Coronado Airport at the time of the accident.

The pilot reported that, during the takeoff roll on runway 17, he "noticed a flat spot in the power" as he opened the throttle. He verified that the propeller was set "for fine pitch" and "noticed the rpm showed 2400 rpm" instead of the expected 2500 rpm. At an airspeed of 80 mph, the pilot "rotated into a climb." After retracting the landing gear, he "felt the climb cease and the aircraft started to settle." Since there was "insufficient remaining runway to attempt to abort," the pilot turned left intending to land gear-up on an east/west dirt road south of the airport. The airplane touched down south of the road, the left wing struck "a piece of concrete debris which turned the aircraft 90 degrees to the left and caused the aircraft to settle on the road."

A field inspection of the airplane and engine was conducted by FAA personnel. The inspection revealed that the fuselage was distorted. The reason for the loss of engine power could not be determined.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# FTW96LA169