N6292B

Substantial
Minor

DICKINSON FISHER CLASSIC S/N: 001

Accident Details

Date
Saturday, May 25, 1996
NTSB Number
CHI96LA178
Location
MOORESVILLE, IN
Event ID
20001208X05734
Coordinates
39.609561, -86.370849
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
0
Total Aboard
1

Probable Cause and Findings

the pilot failed to maintain adequate altitude and clearance from the trees, and had made an improper in-flight decision when he got to far from a suitable landing area. The reason for the loss of power failure was undetermined.

Aircraft Information

Registration
N6292B
Make
DICKINSON
Serial Number
001
Engine Type
Turbo-shaft
Model / ICAO
FISHER CLASSIC A270
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
DICKINSON JAMES A
Address
1015 N INDIANA ST
Status
Deregistered
City
MOORESVILLE
State / Zip Code
IN 46158-1037
Country
United States

Analysis

On May 25, 1996, at 1540 eastern daylight time, an experimental Fisher Classic, N6292B, sustained substantial damage when it hit trees during a forced landing due to loss of engine power. The commercial pilot received minor injuries. The 14 CFR 91 flight departed Mooresville, Indiana, on a local flight. Visual meteorological conditions prevailed and no flight plan was filed.

The pilot reported that it was the first flight of his home built airplane. He reported that he had built the aircraft himself, and bought a used aircraft engine which had 211 total hours on it. He installed a new aviation certified fuel pump on the engine before the flight. The aircraft had been registered with the Federal Aviation Administration (FAA). However, it had not been inspected for airworthiness by the FAA and had not been certified prior to the first flight.

The pilot reported that during the preflight all instruments checked normal. He reported that the aircraft was sluggish in the climb. He climbed to 700 feet above ground level (AGL) and flew for 12 minutes, and then the engine quit. He reported that he could not get to an open field, and landed in a wooded area. He reported the airplane landed in the trees which cushioned the impact with the ground.

The pilot reported that he thought the engine had seized. He also indicated that he thought the prop had been set at too high a pitch, 14 degrees, and it may have required the engine to work too hard to maintain flight. He reported that he could not get the engine to produce more than 6000 RPM's at full throttle. He reported that he had been at full throttle for the entire 12 minutes.

The examination of the aircraft revealed that the engine had not seized. The pistons and cylinder walls were examined for overheating or seizure, and none was found. The carburetors were disassembled and no discrepancies were found. The exhaust manifold was removed and the were no indications of a rich fuel mixture or scored pistons. The fuel tank was inspected and no discrepancies were found. The fuel pump was inspected and it was determined that the pump was an aviation fuel pump with the designed "weep hole." However, the fuel pump's inlet and impulse hoses had sharp bends in them. The prop was rotated and the engine exhibited continuity.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI96LA178