N48518

Substantial
None

Grumman-Schweizer G-164B S/N: 61B

Accident Details

Date
Saturday, May 25, 1996
NTSB Number
CHI96LA186
Location
CROOKSTON, MN
Event ID
20001208X05739
Coordinates
47.769977, -96.599380
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

catastrophic engine failure.

Aircraft Information

Registration
N48518
Make
GRUMMAN-SCHWEIZER
Serial Number
61B
Engine Type
Turbo-shaft
Year Built
1976
Model / ICAO
G-164B G64T
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
GASPER AIR SPRAY INC
Address
BOX 276
Status
Deregistered
City
CROOKSTON
State / Zip Code
MN 56716
Country
United States

Analysis

On May 25, 1996, at 0830 central daylight time, a Grumman G-164-B airplane, N48518, operated by Gasper Airspray, Inc., sustained substantial damage when it nosed over during a forced landing, following a total loss of engine power, near Crookston, Minnesota. The solo commercial pilot reported no injuries. The aerial application flight originated about 0800 and was conducted under 14 CFR Part 137. A flight plan was not filed for the local flight and visual meteorological conditions prevailed.

The pilot reported that he was at 200 feet turning for a spray run and the engine began "running very rough, some smoke and oil noticed." He conducted a forced landing in an "open, rough field which had recently been saturated with heavy rain fall. Upon touch down, the main wheels began sinking in the mud and caused the aircraft to slowly flip forward...."

The Federal Aviation Administration Inspector who examined the airplane reported that it was moved prior to his arrival at the accident site. He reported that the engine had failed catastrophically. He observed five cracked cylinders and suspected a master rod failure.

The owner of the airplane reported that the engine had been run about 100 hours since overhaul. He said that there was oil on the ground in the vicinity of the accident site and that he was confident the engine was properly serviced with oil prior to the flight. He reported that examination of the propeller governor was conducted by an FAA approved repair station which reported the governor was servicable.

The engine was examined by an FAA approved engine overhaul facility. The chief inspector reported that "master rod bearing failure typical of oil starvation had occurred.... The damage found during disassembly was typical of other engines known to have been oil starved during operation. The cause of oil starvation in this engine is unknown."

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI96LA186