N58KD

Substantial
None

Beech 58 S/N: TH-895

Accident Details

Date
Saturday, May 18, 1996
NTSB Number
LAX96LA198
Location
LOS ANGELES, CA
Event ID
20001208X05812
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
3
Total Aboard
3

Probable Cause and Findings

an interruption of fuel flow to the right engine for undetermined nonmechanical reasons. A contributing factor was the pilot's failure to keep the right engine's propeller feathered which reduced the airplane single engine performance capabilities.

Aircraft Information

Registration
N58KD
Make
BEECH
Serial Number
TH-895
Engine Type
Reciprocating
Model / ICAO
58 BE58
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
DIDDEN GARY E
Address
2903 ALTA TERRACE
Status
Deregistered
City
LA CRESCENTA
State / Zip Code
CA 91214
Country
United States

Analysis

HISTORY OF FLIGHT

On May 18, 1996, at 1144 hours Pacific daylight time, a Beech 58, N58KD, owned and operated by the pilot, experienced a loss of right engine power during takeoff from the Whiteman Airport, Los Angeles, California. The airplane collided with terrain near the airport and was substantially damaged. Neither the private pilot nor the two passengers were injured. Visual meteorological conditions prevailed at the time of the personal flight which was originating at the time of the accident.

The local air traffic controller reported that seconds after the airplane became airborne from runway 12, the pilot reported he was losing power in his right engine. The controller cleared the pilot to land using any runway. The controller stated that he did not hear an acknowledgment from the pilot, but he did observe the airplane in a descending right turn. The pilot made a forced landing in rough terrain near the 15th hole of the Hanson Dam golf course.

In the pilot's completed accident report, he indicated that in preparation for his personal flight to Santa Ynez with his wife and daughter, he had arrived at the Whiteman Airport around 1100. Sixty gallons of fuel were added (30 gallons per wing tank) to the hangared airplane, and the three fuel sumps were drained with no evidence of contaminants.

The pilot further reported that both engines started normally, and no discrepancies were observed during the pre-takeoff engine and propeller checks. The pilot reported that during takeoff the airplane "lifted off the runway at the same approximate location we normally do," a positive rate of climb was established, and the landing gear was retracted. Suddenly and without warning, the right engine lost all power, and the right engine's fuel flow indicator read 0 gallons per hour. The pilot turned on the fuel boost pump for the right engine, but the engine did not restart. The pilot said he then feathered the right engine's propeller, made a slight left turn toward the golf course, and tried to maintain altitude. The pilot further reported that he then unfeathered the right engine's propeller, pushed the right throttle forward and turned the boost pump on (again). None of these actions restored the engine's power, and the airplane did not maintain altitude.

TESTS AND RESEARCH

Federal Aviation Administration (FAA) airworthiness inspectors reviewed the airplane's maintenance records and examined the airframe and engine. The FAA found no evidence of fuel contamination, and reported that the "aircraft tear down revealed no abnormal conditions or findings."

The following right engine components were removed and examined under FAA supervision: the fuel pump and drive coupling; the throttle/fuel control metering unit; the manifold valve; and the injector lines and nozzles. Following the examinations, the FAA reported that no discrepancies were found with any of these components.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX96LA198