N88401

Substantial
None

Bellanca 8GCBC S/N: 122-75

Accident Details

Date
Sunday, June 2, 1996
NTSB Number
SEA96LA109
Location
RICHLAND, WA
Event ID
20001208X06105
Coordinates
46.249843, -119.290008
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

the pilot's failure to perform a go-around and his subsequent excessive use of the aircraft brakes. The short airstrip length and the pilot's excessive airspeed for the approach were related factors.

Aircraft Information

Registration
Make
BELLANCA
Serial Number
122-75
Engine Type
Reciprocating
Year Built
1974
Model / ICAO
8GCBC BL8
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
3
FAA Model
8GCBC

Registered Owner (Current)

Name
KIMBALL CLAYTON SCOTT
Address
207 KRANICHWOOD CT
City
RICHLAND
State / Zip Code
WA 99352-9498
Country
United States

Analysis

On June 1, 1996, at approximately 1830 Pacific daylight time, a Bellanca 8GCBC, N88401, sustained substantial damage when it nosed over during landing on a private 1,000-foot gravel strip near Richland, Washington. The commercial pilot/owner, who was the aircraft's sole occupant, was not injured. Visual meteorological conditions prevailed at the time of the accident and no flight plan was filed for the 14 CFR 91 flight from Stehekin State Airport, Stehekin, Washington.

The pilot reported:

I made an approach for a landing to the west. Was a little hot (short final approximately 62 mph indicated) and touched down approximately 150-200 feet past the beginning of the strip; I considered a go-around but thought I still had distance remaining to stop....I pulled the flaps to put more load on the wheels and applied brakes; it was not slowing like I thought it should. I considered a go-around at this point but was not certain that I would be able to clear the trees at the west end of the strip, thus I applied more brake at which time the tail came up. Although I...came off the brakes...I was unable to get the tail back down at which point I hit the softer dirt on the left side of the gravel....the aircraft [pitched] farther forward...and then the aircraft continued over onto its back and came to rest.

The pilot stated in his report that the wind sock at the airstrip indicated a right quartering head wind of about 5 knots at the time of the accident. The pilot made the following recommendation in his report as to how the accident could have been prevented: "Go around could have been made on very short final or immediately upon touch[down]."

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# SEA96LA109