N2145D

Substantial
None

Beech 35 S/N: D3490

Accident Details

Date
Monday, June 10, 1996
NTSB Number
SEA96LA121
Location
AURORA, OR
Event ID
20001208X06116
Coordinates
45.229980, -122.800857
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

failure of the non-certificated pilot to ensure that the landing gear was properly extended for landing. The non-certificated pilot's diverted attention was a related factor.

Aircraft Information

Registration
N2145D
Make
BEECH
Serial Number
D3490
Engine Type
Reciprocating
Year Built
1953
Model / ICAO
35 BE35
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
KELLY FRANCIS L
Address
1532 US 41 BYPASS S PMB 230
Status
Deregistered
City
VENICE
State / Zip Code
FL 34293
Country
United States

Analysis

On June 9, 1996, at approximately 2100 Pacific daylight time, N2145D, a Beech 35, sustained substantial damage in a wheels-up landing at Aurora State Airport, Aurora, Oregon. The aircraft was being operated under 14 CFR 91 on a local flight out of Aurora. The non-certificated pilot (who owned the aircraft but had not registered it to his name since purchasing it in approximately January 1994) and a pilot-rated passenger (who holds a commercial pilot certificate but did not hold a current medical certificate at the time of the accident) were not injured. Visual meteorological conditions prevailed at the time of the accident and no flight plan had been filed.

In a telephone interview with an FAA inspector in the Hillsboro, Oregon, Flight Standards District Office (FSDO), the pilot/owner stated that his passenger was acting as pilot-in-command and was flying the aircraft at the time of the accident. However, the passenger stated to investigators that he was not flying the aircraft at the time of the accident, and that he had been unaware that the pilot/owner of the aircraft did not hold a pilot certificate. He said that he would not have flown with the pilot/owner if he had known the pilot/owner did not have a license. The passenger also stated that he did not touch the aircraft controls "except to save my life when I realize[d] the gear was retracted on touchdown." The pilot/owner indicated on his accident report that he occupied the left seat, with the pilot-rated passenger in the right seat of the aircraft.

Both occupants stated to the FAA inspector that while in the traffic pattern, their attention was diverted while searching for another aircraft which called inbound to Aurora on an instrument approach and reported being at their altitude. The passenger stated that the gear was initially down and that the pilot/owner raised the gear during the search for the other aircraft. The pilot/owner stated that he thought the passenger "cycled the landing gear twice" before the accident. The passenger, who also is a Bonanza owner and has logged about 2,500 hours of pilot time, said that as the pilot/owner began the landing flare he could tell by the speed and pitch attitude that the gear had not been extended. He said that when the tail touched, he reached forward and pulled back on the yoke in order to cushion the contact with the runway. The aircraft then slid to a stop on the runway on its belly. According to the passenger, he did not realize the pilot/owner did not hold a pilot certificate until he was advised of that situation after the accident. No problems were found in the aircraft's gear extension system, and neither occupant claimed that there had been any malfunction.

According to copies of the aircraft logbook, the aircraft's last annual inspection, dated April 15, 1996 at 3,452.0 tachometer hours, was signed off as: "This aircraft has been inspected IAW an annual inspection and a list of discrepancies dated 1-2-96 has been provided to the aircraft owner." The logbook entry indicated that per FAA Airworthiness Directive (AD) 62-08-03, cracks were found but no further action was taken. This AD mandates inspection of certain type control wheels for cracks every 100 hours in service or 12 calendar months, and specifies that if cracks are found, the control wheels are to be replaced before further flight. Although a subsequent aircraft logbook entry, dated May 24, 1996 at 3,455 tachometer hours, indicated that a "loaner dual control yoke" had been installed by Flightcraft, Inc. of Portland, Oregon, no further evidence was provided to indicate that the aircraft had been signed off as airworthy, based on annual inspection, within the 12 months prior to the accident.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# SEA96LA121