N5335B

Substantial
Minor

Cessna 182 S/N: 33335

Accident Details

Date
Saturday, July 20, 1996
NTSB Number
CHI96LA248
Location
ROSE HILL, KS
Event ID
20001208X06185
Coordinates
37.560909, -97.129432
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
0
Total Aboard
1

Probable Cause and Findings

the worn carburetor, and inadequate inspection of the aircraft by other maintenance personnel.

Aircraft Information

Registration
N5335B
Make
CESSNA
Serial Number
33335
Engine Type
Reciprocating
Year Built
1956
Model / ICAO
182 C182
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
SALE REPORTED
Address
145 J V WALKER ST
Status
Deregistered
City
ELY
State / Zip Code
NV 89301-2054
Country
United States

Analysis

On July 20, 1996, at 1000 central daylight time, a Cessna 182, N5335B, sustained substantial damage during a forced landing following a loss of engine power. The commercial pilot reported minor injuries. The airplane was conducting local parachute jumping activities under provisions of 14 CFR Part 91. The airplane was returning to the airport when the accident occurred. The pilot was the only occupant. No flight plan was on file. Visual meteorological conditions prevailed. The flight departed at 0930.

The pilot stated that while in a descent she was maintaining 15 inches of manifold pressure. When she attempted to increase power the engine "stopped." She said she conducted a forced landing to an open field. The airplane struck a wire prior to touchdown where the nose landing gear dug in the soft terrain and the airplane nosed over.

Subsequent to the accident the carburetor was examined and a visual inspection revealed excessive mixture lever wear. The wear resulted in excessive travel and binding of the lever with the cable. The throttle shaft was found worn as was the pin in the metering rod. An "o" ring on the mixture rod was missing. The valve and seat were sticking and the float adjustment was higher than specifications. The accelerator pump was worn as was the accelerator pump lever. The total time in service for the engine was 2,384 hours. The total time in service for the carburetor was not determined. The most recent inspection of the airplane was on October 1, 1995. The airplane had operated 224 hours since the inspection.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI96LA248