N6087N

Destroyed
None

Beech B23 S/N: M-1179

Accident Details

Date
Friday, August 9, 1996
NTSB Number
LAX96LA302
Location
MODESTO, CA
Event ID
20001208X06549
Coordinates
37.629306, -120.969512
Aircraft Damage
Destroyed
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

fuel starvation due to the pilot's inadequate fuel management and failure to reposition the fuel selector to a tank containing adequate fuel. The power lines were a factor.

Aircraft Information

Registration
N6087N
Make
BEECH
Serial Number
M-1179
Engine Type
Reciprocating
Year Built
1968
Model / ICAO
B23 BE23
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
BAKER JILL A
Address
1640 CABLE ST
Status
Deregistered
City
SAN DIEGO
State / Zip Code
CA 92107
Country
United States

Analysis

On August 9, 1996, at 1305 hours Pacific daylight time, a Beech B23, N6087N, owned and operated by the pilot, experienced a total loss of engine power during a go-around which followed an intentionally performed low pass over the Modesto City Airport, Modesto, California. When the engine lost power, the airplane was between 600 and 900 feet above ground level. The pilot reported that she made a forced landing on a street, but during the approach collided with power lines. As the airplane slid to a stop a fuel-fed fire erupted, which ultimately destroyed the airplane. Neither the private pilot nor the passenger were injured during the Palms-to-Pines air race. The low pass was performed for timing purposes. Visual meteorological conditions prevailed, and a visual flight rules flight plan was filed. The flight originated from Santa Monica, California, at 1050.

The pilot reported that upon departure the fuel tanks were full. The two wing tanks each held about 28.8 gallons of fuel. Fuel can only be used from one of the tanks at a time since there is no "both" fuel tank selector position. The pilot stated that she did not recall repositioning the fuel selector during the 2:10 hour-long flight. The pilot additionally reported that she anticipated the engine would use about 11.9 gallons per hour during the air race.

Airplane recovery personnel reported that they examined the engine. Compression was obtained in all cylinders. The carburetor fuel screen was found clean. All of the spark plugs appeared to be in a serviceable condition. Spark was obtained upon rotation of the magneto drive gears.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX96LA302