N1368Z

Substantial
None

Beech BE-35 S/N: D-6789

Accident Details

Date
Monday, September 23, 1996
NTSB Number
CHI96LA343
Location
MINOT, ND
Event ID
20001208X06701
Coordinates
48.230098, -101.289070
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
4
Total Aboard
4

Probable Cause and Findings

fuel management was not performed and starvation of the fuel system. A factor involved was inadequate in-flight planning/decision.

Aircraft Information

Registration
N1368Z
Make
BEECH
Serial Number
D-6789
Engine Type
Reciprocating
Model / ICAO
BE-35 BE35
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
GOWAN DAVID C
Address
2405 13TH ST SE RR 7
Status
Deregistered
City
MINOT
State / Zip Code
ND 58701
Country
United States

Analysis

On September 22, 1996, at 2030 central daylight time (cdt), a Beech BE-35, N1368Z, owned and operated by an instrument rated private pilot, was substantially damaged during a forced landing, while on a two mile final approach to runway 26, at Minot International Airport, Minot, North Dakota, following a loss of engine power. The pilot and three passengers reported no injuries. Visual meteorological conditions prevailed at the time of the accident. The personal 14 CFR Part 91 flight was not operating on a VFR flight plan. The flight departed Holman Field, Saint Paul, Minnesota at 1730 cdt.

According to the pilot's written statement, while on a three mile base leg turning onto final approach to runway 26, the pilot noticed that the engine sputtered and lost total power. The pilot switched the fuel selector to the right fuel tank and was unsuccessful on an engine restart. He set up a 65 mph glide slope and landed 2 1/4 mile short of runway 26.

The North Dakota Highway Patrol received a written statement form the pilot at the time of the accident. According to the Highway Patrol Officer, who took a statement from the pilot, "...it took 33 gallons to fly to Minneapolis and he had bucked a 15 mph wind on the return flight and forgot to switch the tank to the right one before he ran out. He stated he always does it, but forgot this time. He stated it was pilot error."

A Federal Aviation Administration Maintenance Inspector blocked the nose of the airplane up and cranked the engine through a couple of times and the engine started. The engine ran normal with no discrepancies noticed.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI96LA343