N4533H

Substantial
None

Air Tractor AT-502 S/N: 502-0105

Accident Details

Date
Tuesday, October 8, 1996
NTSB Number
FTW97LA012
Location
IDALOU, TX
Event ID
20001208X06878
Coordinates
33.659553, -101.680793
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

the pilot's improper planning/decision, which resulted in an overrun during takeoff and an encounter with cotton (crop) and rough/uneven terrain. Factors relating to the accident were: the excessive loading of the airplane for the existing conditions, the short runway, the high density altitude, and the pilot's delay in jettisoning the load.

Aircraft Information

Registration
N4533H
Make
AIR TRACTOR
Serial Number
502-0105
Engine Type
Turbo-shaft
Model / ICAO
AT-502 AT5T
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
NORTH STAR AVIATION INC
Address
PO BOX 248
Status
Deregistered
City
JOHNSON
State / Zip Code
KS 67855-0248
Country
United States

Analysis

On October 8, 1996, at 1745 central daylight time, an Air Tractor AT-502, N4533H, was substantially damaged during takeoff from a private airstrip near Idalou, Texas. The airplane, owned and operated by Everitt Aerial Spraying Inc., was being operated under Title 14 CFR Part 137 at the time of the accident. The commercial pilot, sole occupant of the airplane, was not injured. Visual meteorological conditions prevailed for the flight for which a flight plan was not filed. The flight was originating at the time of the accident.

According to the FAA inspector, the pilot was attempting to depart his 2,300 foot long dirt airstrip with a 3,040 pound payload of cotton defoliant for a local aerial application flight. The pilot told the FAA inspector that the airplane failed to become airborne and overran the departure end of the airstrip impacting furrows perpendicular to the aircraft takeoff path.

In the narrative portion of the enclosed NTSB Form 6120.1/2, the pilot stated that "the gross weight of the airplane exceeded the ability of the aircraft to become airborne within the length of the runway." The pilot added that "attempts to jettison the load near the end of the strip were not in sufficient time to time to prevent running off the end of the runway."

During a telephonic interview with the investigator-in-charge, the pilot stated that he had been operating from the same runway with a 350 gallon load (500 gallon hopper) all afternoon. The pilot stated that he was aware that the chemical being sprayed on the last flight was changed over to a heavier chemical, and he expected the takeoff roll to increase by another 50 to 100 yards. He added that the airplane managed to break ground as he anticipated, but the wheels of the airplane dragged on the cotton plants and eventually decelerated the airplane to the point where the flight could not be maintained.

Examination of the airplane by the FAA inspector revealed that the left main landing gear collapsed and the left wing sustained structural damage. The flaps were found in the retracted position; however, the pilot stated that he used flaps for takeoff and he retracted them prior to exiting the airplane.

Based on figures provided by the operator, the density altitude at the time of the accident was calculated at 9,500 feet. The approved airplane flight manual does not provide any performance data on the required takeoff roll for this flight.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# FTW97LA012