N4523V

Substantial
None

Beech 35 S/N: D-1346

Accident Details

Date
Wednesday, November 27, 1996
NTSB Number
ATL97LA027
Location
LAFAYETTE, GA
Event ID
20001208X06996
Coordinates
34.699676, -85.279685
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
3
Total Aboard
3

Probable Cause and Findings

failure of maintenance personnel to balance the ruddervator assemblies after they had been reskinned and painted, which resulted in flutter and subsequent damage to the empennage.

Aircraft Information

Registration
N4523V
Make
BEECH
Serial Number
D-1346
Engine Type
Reciprocating
Year Built
1948
Model / ICAO
35 BE35
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
REGISTRATION PENDING
Address
PO BOX 112
Status
Deregistered
City
MAYSEL
State / Zip Code
WV 25133-0112
Country
United States

Analysis

On November 27, 1996, at 1600 eastern standard time, a Beech 35, N4523V, experienced the failure of the aft bulkhead in the empennage section of the airframe while at cruise flight near Lafayette, Georgia. The personal flight operated under the provisions of Title 14 CFR Part 91 with no flight plan filed. Visual weather conditions prevailed at the time of the accident. The airplane sustained substantial damage. The pilot-in -command ,the pilot/passengers, and the passenger were not injured. The flight departed Lafayette, Georgia, at 1550.

The two pilots reported that ten minutes into the flight they experienced flutter in the aft section of the airframe. The flutter episode last about three seconds. The pilot immediately reduced engine power, and the flutter episode stopped. The pilot elected to return to the airport in Lafayette and landed without incident. The visual examination of the empennage section disclosed that the airframe had sustained structural damage that wrinkled the skin in the vicinity of both ruddervator and stabilizer assemblies.

An examination of the internal structural components of the empennage disclosed that the bulkhead at fuselage station (FS) 256.9 exhibited cracks at the four corners of the assembly. In the immediate vicinity of the damaged bulkhead, there was buckling to the aft fuselage skin. The remainder of the aft portion of the empennage was not damaged, including the ruddervator assemblies.

The ruddervators were removed from the airframe and balance checked in accordance with the Bonanza 35 series Shop Manual. The left and right ruddervators exhibited static underbalance moments of 23.73 and 22.95 inch-pounds respectively. The required static balance range is 16.80 to 19.80 inch pounds. When the screws that attached the counterbalance assemblies to the ruddervator were removed, there was a top coat paint seal that covered the screw heads.

A review of the airframe maintenance logs disclosed that the last ruddervator painting and balancing were accomplished on January 24, 1987. The maintenance log review also failed to disclose the completion of Airworthiness Directive (AD) 94-20-04, that required a balance check of the ruddervator assemblies within the next one hundred hours time-in-service after the effective date of this AD (see attached AD-94-20-04).

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ATL97LA027