N74HL

Destroyed
None

Bell TH-13T S/N: 3652

Accident Details

Date
Monday, April 7, 1997
NTSB Number
FTW97TA154
Location
CAPITAN, NM
Event ID
20001208X07719
Coordinates
33.540557, -105.590354
Aircraft Damage
Destroyed
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

loss of engine power for undetermined reason(s).

Aircraft Information

Registration
N74HL
Make
BELL
Serial Number
3652
Year Built
2001
Model / ICAO
TH-13T

Registered Owner (Historical)

Name
SALE REPORTED
Address
PO BOX 157
Status
Deregistered
City
NEWPORT
State / Zip Code
MN 55055-0157
Country
United States

Analysis

On April 7, 1997, approximately 0815 central daylight time, a Bell TH-13T helicopter, N74HL, owned and operated by the pilot, was destroyed following a loss of power and subsequent forced landing near Capitan, New Mexico. Both occupants, the commercial pilot and one passenger, were not injured. Visual meteorological conditions prevailed for the Title 14 CFR Part 91 predator control flight. A flight plan was not filed. The helicopter was airborne for approximately 45 minutes prior to the accident.

The pilot reported that while flying at an altitude of about 35 feet AGL and 30 knots, "a slight shudder was felt in the aircraft as though a change of wind direction had occurred." All instruments and systems "remained in the green and functioning." Several minutes later, a complete engine failure occurred. The pilot recalled hearing a "strange noise" immediately preceding the loss of power. Subsequently, he initiated a low altitude auto rotation. Approximately 10 feet AGL, the aircraft began to turn to the left, and "in order to avoid a roll over", the pilot lowered the collective and informed the passenger of an immanent hard landing. Upon contact with the ground, the main rotor contacted and severed the tail boom. Immediately following the hard landing, a fire started in the engine compartment. Both the pilot and passenger evacuated and the aircraft was consumed by fire.

Examination of the wreckage to discover the cause of the loss of engine power was unsuccessful due to extreme fire damage to the engine, fuel system, and accessories. However, according to the helicopter manufacturer, who assisted in the examination, the post impact fire most likely resulted from the right, external mounted, fuel tank breaking loose from its mounts and dislodging the fuel lines. This allowed fuel to spill onto the hot engine exhaust manifold. The helicopter was not equipped with fiberglass fuel tank straps or self sealing "break away" fuel line fittings.

According to carburetor icing probability charts, the ambient temperature and dew point were conducive to carburetor icing.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# FTW97TA154