N525BB

Substantial
None

Hammer AVID FLYER S/N: 525

Accident Details

Date
Sunday, May 4, 1997
NTSB Number
ANC97LA068
Location
CHITINA, AK
Event ID
20001208X07838
Coordinates
61.449035, -143.150024
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

improper overhaul of the engine, which resulted in a seized piston and resultant loss of engine power. Rough terrain in the emergency landing area was a related factor.

Aircraft Information

Registration
N525BB
Make
HAMMER
Serial Number
525
Engine Type
Reciprocating
Model / ICAO
AVID FLYER BPAT
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
HAMMER ROBERT
Address
1 NAZZINA RD
Status
Deregistered
City
MCCARTHY
State / Zip Code
AK 99588
Country
United States

Analysis

On May 3, 1997, about 1900 Alaska daylight time, a wheel equipped homebuilt, experimental Hammer, Avid Flyer airplane, N525BB, crashed during the initial takeoff climb from the Chitina Airport, Chitina, Alaska. The airplane was being operated as a visual flight rules (VFR) cross-country personal flight to McCarthy, Alaska, when the accident occurred. The airplane, operated by the pilot, sustained substantial damage. The certificated private pilot, the sole occupant, was not injured. Visual meteorological conditions prevailed.

On May 4, 1997, at 1222, the pilot reported in a telephone conversation with the National Transportation Safety Board (NTSB) investigator-in-charge (IIC), that he just departed runway 13 at Chitina and climbed to about 250 feet above the ground. The engine, a Rotax 618, suddenly quit. The pilot made a 180 degree turn to return to the runway. The pilot performed an emergency landing short of the runway into low brush. The airplane received damage to the fuselage and wingtips.

On November 20, 1997, the pilot reported the engine was last overhauled 5 hours before the accident at a facility in Birchwood, Alaska. During the overhaul, one of the engine's two pistons was replaced with an oversize piston. The piston cylinder was also bored oversize. The second engine piston was not replaced, and remained standard size.

After the accident, the pilot sent the engine to an overhaul facility in San Leandro, California. The examination revealed the oversize engine piston was found seized in the cylinder. Measurement of the oversize piston revealed it was the same size as the cylinder bore, both measuring 2.998 inches.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ANC97LA068