N474Y

Substantial
Serious

Grumman G164 S/N: 119

Accident Details

Date
Thursday, May 29, 1997
NTSB Number
CHI97LA150
Location
ILLINOIS CITY, IL
Event ID
20001208X07887
Coordinates
41.399559, -90.900817
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

failure of the pilot to see and maintain clearance from a static wire. The proximity of the wire was a related factor.

Aircraft Information

Registration
N474Y
Make
GRUMMAN
Serial Number
119
Engine Type
Turbo-shaft
Model / ICAO
G164 G64T
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
J P'S AGRICAIR INC
Address
1276 HIGHWAY 94
Status
Deregistered
City
ALEDO
State / Zip Code
IL 61231-8691
Country
United States

Analysis

On May 29, 1997 at 1858 central daylight time (cdt), a Grumman G164, N474Y, was conducting agricultural spraying operations near Illinois City, Illinois, when the airplane hit a static wire, impacted with the terrain and then flipped inverted. The pilot was flying parallel to the power lines during the spraying operations. Witnesses reported that the pilot began a pull up and left turn, when the airplane's left wing tip struck the static line. The commercial rated pilot of the airplane was taken to a local hospital following the accident with serious back injuries. The 14 CFR Part 137 agricultural flight was operating in visual meteorological conditions and no flight plan had been filed for the local flight.

The investigator in charge (IIC) contacted a local volunteer fire chief who had responded to the initial accident call. The fire chief was also a pilot and and he documented the accident site for the IIC. The first pieces of airplane he found in the wreckage path were pieces of left wing leading edge. These leading edge pieces were found very close to the powerlines. The distance from these first pieces to the main wreckage was approximately 130 yards. Just prior to the main wreckage there were ground scar marks which appeared to match the pattern of the airplane's landing gear. Both blades on the propeller were curled back, and one blade's leading edge was jagged along its leading edge. The fire chief believed that the jagged leading edge was caused by the propeller striking a wire. All flight controls appeared to be connected correctly. The cockpit engine controls were found with the throttle in a mid range position, the magnetos were in the both position, the propeller was full forward, and the mixture was full rich. Fuel was found in the airplane's left and center fuel tanks. Fuel was also found in the line which runs from the gascalator to the fuel valve. The fuel valve was found in a position between fuel tanks.

The pilot of the airplane was contacted by telephone on June 12, 1997. The pilot of the accident aircraft reported to the IIC that there were no discrepancies with the airplane or the engine before the accident. The pilot said that he just did not see the wire which the airplane hit.

The airplane's left wing struts were broken, the vertical fin, rudder and upper wing were crushed.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI97LA150