N7684V

Substantial
None

Aero Commander CALLAIR A-9B S/N: 1432

Accident Details

Date
Monday, June 23, 1997
NTSB Number
FTW97LA232
Location
EL INDIO, TX
Event ID
20001208X08129
Coordinates
28.509679, -100.309486
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

the pilot's inadequate preflight, subsequent fuel starvation, and failure of the pilot to reposition the fuel selector to another tank (perform emergency procedure) after the loss of engine power, which resulted in a forced landing and subseqent nose-over. Factors relating to the accident were: false fuel quantity indication, and the lack of suitable terrain for an emergency landing.

Aircraft Information

Registration
N7684V
Make
AERO COMMANDER
Serial Number
1432
Engine Type
Turbo-jet
Year Built
1968
Model / ICAO
CALLAIR A-9B L29
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
HUNTER JAMES ROGERS
Address
100 WILL ROGERS DR
Status
Deregistered
City
SCHERTZ
State / Zip Code
TX 78154-1023
Country
United States

Analysis

On June 23,1997, approximately 0805 central daylight time, a Callair A-9B agricultural airplane, N7684V, was substantially damaged during a forced landing following a total power loss near El Indio, Texas. The commercial pilot, sole occupant in the airplane, was not injured. The airplane was owned/operated by a private individual under Title 14 CFR Part 137. Visual meteorological conditions prevailed for the aerial application flight which had originated from a private airstrip approximately 5 minutes before the accident. No flight plan had been filed for the flight.

According to the pilot, he was working on a boll weevil eradication contract. He stated that he had been servicing the airplane (with fuel, oil, and applicant) at the end of each day. He reported that the day before the accident he was distracted from his servicing process by the arrival of a customer and the news of a family problem. The pilot reported that the next morning, while doing the preflight of the airplane, "I checked the sumps but did not remove the fuel caps to visually check the fuel [quantity]."

The pilot reported that he departed for the first flight of the day with the fuel selector on the right fuel tank; this was the fuel tank which was not serviced the day before. The pilot further reported that the right fuel gage indicated "full." While making his first application swath, the engine "quit." The pilot "saw the fuel pressure light come on and he turned on the boost pump"; he "delayed switching fuel tanks because he thought he had full tanks on both sides and that there was some other problem."

The pilot performed a forced landing to a cotton field. He stated that "I got down as smooth and slow as I could but the wheels got down into the mud and it flipped over." The airplane came to rest tail first in the inverted position.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# FTW97LA232