N85NW

Substantial
None

Garlick UH-1H S/N: 66-0792

Accident Details

Date
Tuesday, June 3, 1997
NTSB Number
SEA97LA126
Location
ADDY, WA
Event ID
20001208X08244
Coordinates
48.320243, -117.909606
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The inflight failure of the K-FLEX engine-to-gear box drive shaft and no suitable site in which to make a forced/emergency landing. A factor was the mountainous/hilly terrain.

Aircraft Information

Registration
N85NW
Make
GARLICK
Serial Number
66-0792
Engine Type
Reciprocating
Model / ICAO
UH-1H SA02
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Analysis

On June 3, 1997, approximately 0630 Pacific daylight time, a Garlick UH-1H helicopter, N85NW, collided with the terrain during a forced landing near Addy, Washington. The commercial pilot, who was the sole occupant, was not injured, but the aircraft, which was being operated by Northwest Helicopters, Inc., sustained substantial damage. The 14 CFR Part 133 logging flight, which had been in the air about 30 minutes, was being conducted in visual meteorological conditions, and no flight plan had been filed.

According to the pilot, he was about 30 minutes into the first logging cycle of the day, and was heading back to the hooker to pick up another log when the accident sequence began. He said that suddenly he "...heard a high-speed shredding sound with accompanying high-frequency vibration." He immediately lowered the collective, released the 150 foot long-line (which was not attached to any load), and checked the RPM and all other instruments. He said that all the instruments looked normal, but because the sound and vibration were quickly getting worse, he headed downhill over the 130 foot high trees in hopes of finding a location where an emergency landing could be made. While heading downhill, he heard a second loud noise, which he suspected was the failure of some part of the main rotor drive shaft system. Immediately after hearing the second noise, the rotor RPM began to decay, and the pilot "...stretched the downhill glide over a last group of trees, and fell into a switchback road." As the aircraft fell onto the road it "...hit four small trees in the process of crash landing." Upon hitting the terrain, the aircraft pitched up on its nose, whereupon the main rotor severed the tail boom.

After the accident a number of the flex bands on the K-FLEX drive shaft, which is located between the engine and transmission, where found to have failed. The shaft and as many of the flex band sections as could be found at the accident site were sent to the NTSB metallurgical laboratory in Washington, D.C., in order for all fracture surfaces to be examined. That examination found that "One fracture on a rectangular flex leg section showed evidence of preexisting cracking in the form of a fatigue crack region." All the remaining fractures were either damaged so severely during the accident that the original fracture surface could not be viewed, or displayed characteristics of a "...complete overstress separation."

A review of the K-FLEX shaft's records revealed that this shaft had originally been used by the United States Army. Army records show that the shaft was removed from an AH-1F (attack model) helicopter when the shaft had accumulated a total of 459 hours since new. It was then released to the civilian market, and accumulated another 432 hours in logging operations prior to failure. The records also indicated that prior to being put into civilian service, the entire shaft was inspected in accordance with Technical Manual 55-1520-210-23.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# SEA97LA126