N321RM

Substantial
None

Mooney M20K S/N: 25-0230

Accident Details

Date
Friday, August 8, 1997
NTSB Number
LAX97LA282
Location
LAKEPORT, CA
Event ID
20001208X08675
Coordinates
35.310749, -120.269943
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

the pilot's inadequate preflight by failing to ensure that the fuel selector was positioned to a tank containing fuel, which resulted in fuel starvation, and a forced landing shortly after takeoff.

Aircraft Information

Registration
Make
MOONEY
Serial Number
25-0230
Engine Type
Reciprocating
Year Built
1979
Model / ICAO
M20K M20T
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
M20K

Registered Owner (Current)

Name
BIGLER & ASSOCIATES AVIATION INC
Address
3096 BOEING RD
City
CAMERON PARK
State / Zip Code
CA 95682-7831
Country
United States

Analysis

On August 8, 1997, at 1115 hours Pacific daylight time, a Mooney M-20K, N321RM, collided with the ground following a loss of engine power during the takeoff initial climb from the Lakeport, Californa, airport. The aircraft was on a test flight following completion of maintenance. Visual meteorological conditions prevailed at the time and no flight plan was filed. The aircraft incurred substantial damage. The commercial pilot/mechanic, the sole occupant, was not injured. The flight was originating at the time of the occurrence.

In a telephone interview, the pilot/mechanic stated that the aircraft was in the shop to have the left fuel tank resealed. During the procedure, all fuel was drained from the tank, and, none was put in before the test flight. After the work, the pilot/mechanic was departing on a test flight to return the aircraft to service. He stated he is positive the fuel selector was placed on the right tank, which was nearly full. Engine start, taxi, run-up, and the takeoff were normal. In the initial climb, the engine lost power and he could not return to the runway. The aircraft landed in a field and sustained substantial wing damage. He stated his belief that the fuel selector may have been leaking air into the fuel lines from the left tank.

An Federal Aviation Administration airworthiness inspector from the Sacramento, California, Flight Standards District Office examined the aircraft. He reported that the left tank was completely empty and that abundant fuel was present in the right tank. The fuel line into the distributor manifold was loosened and the electric fuel pump energized; air came out of the line at first, followed by a steady stream of fuel. The line was then reconnected. Using the aircraft systems and right tank fuel, the engine was then started and ran satisfactorily.

The pilot/mechanic declined to submit a written statement or complete a Safety Board Pilot/Operator Accident Report.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX97LA282