N8075K

Substantial
None

Grumman-Schweizer G-164B S/N: 560B

Accident Details

Date
Monday, September 1, 1997
NTSB Number
FTW97LA335
Location
MARKSVILLE, LA
Event ID
20001208X08836
Coordinates
31.120929, -92.059776
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The pilot's inadvertent stall during a turn to reverse direction during an aerial application flight. A factor was the pilot's chronic fatigue as result of cumulative long workdays.

Aircraft Information

Registration
N8075K
Make
GRUMMAN-SCHWEIZER
Serial Number
560B
Engine Type
Turbo-shaft
Model / ICAO
G-164B G64T
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
AMERICAN AGVIATION INC
Address
PO BOX 482
Status
Deregistered
City
WALNUT RIDGE
State / Zip Code
AR 72476-0482
Country
United States

Analysis

On September 1, 1997, at 0830 central daylight time, a Grumman-Schweizer G-164B agricultural airplane, was substantially damaged following a loss of control while maneuvering near Marksville, Louisiana. The commercial pilot, sole occupant of the airplane, was not injured. The airplane was owned and operated by the pilot. Visual meteorological conditions prevailed for the Title 14 CFR Part 137 aerial application flight for which a flight plan was not filed. The airplane departed from an airstrip near Vick, Louisiana, approximately 30 minutes prior to the accident.

According to the FAA inspector who traveled to the accident site, the pilot was in the process of executing a turn to reverse direction upon completion of an aerial application pass, when the airplane stalled. Subsequent to the loss of control, the airplane impacted the ground in a left wing low and nose down attitude and came to rest in an open pasture.

Examination of the wreckage by the FAA inspector revealed that both top wings and the main landing gear assembly incurred sustained structural damage. In the enclosed pilot/operator report, the pilot acknowledged that there was no mechanical malfunction prior to the loss of control. In the same document the pilot reported that in the 90 days preceding the accident, he had accumulated 500 hours of flight time.

In a telephonic interview conducted by the investigator in charge, the pilot stated that the accident occurred during the first flight of the day. He added that in the morning of the accident "he felt refreshed and alert following a good night's sleep." He further stated that "his work days for the previous 4 to 5 months had been long, normally working long days from sunrise to sunset" spraying the rice and cotton crops, as well as the boll weevil infestation. The pilot further stated that "the fact that he was trying to do too much probably caught up with him" since he had gone from one contract to the other without rest.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# FTW97LA335