N1668P

Substantial
Serious

Piper PA-18-150 S/N: 18-3797

Accident Details

Date
Saturday, November 15, 1997
NTSB Number
SEA98LA014
Location
BATTLE GROUND, WA
Event ID
20001208X09246
Coordinates
45.800334, -122.479202
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
1
Uninjured
0
Total Aboard
2

Probable Cause and Findings

The owner/pilot's failure to properly install the fuel selector valve after removal, subsequently leading to a false indication on the valve selector handle. This led to the pilot unintentionally closing the valve and starving the engine of fuel during the initial climb.

Aircraft Information

Registration
Make
PIPER
Serial Number
18-3797
Engine Type
Reciprocating
Year Built
1955
Model / ICAO
PA-18-150 PA18
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
PA-18-150

Registered Owner (Current)

Name
PROFESSIONAL PILOTS INC
Address
12304 W 165TH AVE
City
LOWELL
State / Zip Code
IN 46356-9328
Country
United States

Analysis

On November 15, 1997, about 1435 Pacific standard time, N1668P, a Piper PA-18-150, operated by the owner/pilot, collided with trees during a forced landing and was substantially damaged near Battle Ground, Washington. The forced landing was precipitated by a loss of engine power during initial climb after takeoff. The private pilot was seriously injured and his passenger received minor injuries. Visual meteorological conditions prevailed and no flight plan had been filed. The personal flight was conducted under 14 CFR 91.

According to interviews of the pilot that were conducted by the Safety Board (records of interview attached), the pilot stated that on the day of the accident, he departed from his private grass airstrip in Battle Ground and flew to Evergreen Field in Vancouver, Washington, to refuel. He stated that he shut down the airplane when he reached the fuel pump, and he "topped off" both wing fuel tanks himself. He then started the engine without difficulty, and departed from Evergreen Field without performing an engine "run-up." He stated that he then landed back at his grass airstrip, taxied to the end of the strip, and shut down the engine.

The pilot stated that he then boarded his passenger and started the engine after using the engine fuel primer once or twice. He stated that he could remember locking the primer in place after using it. After the engine was started, he took off. As he was climbing about 300 feet per minute, "the fire went out" and the engine "stopped dead." He stated that it did not sputter or cough, it just "went dead."

The pilot stated that he did not attempt to restart the engine, other than moving the fuel selector valve. He stated that he immediately moved the control stick forward to get the nose down. He also remembered that he moved the fuel selector valve from what he thought was the left tank position to the right tank position. He was shown a diagram during the interview of the fuel selector, and indicated that the pointer was the small triangular-shaped pointer opposite of the longer handle (which is the correct indication for the fuel selector).

The pilot further stated that he did not attempt to perform a 180-degree turn, and instead headed toward a clearing in the trees. The airplane struck a tree and this was the last thing that he remembered.

According to a Federal Aviation Administration (FAA) aviation safety inspector from Hillsboro, Oregon, the airplane impacted trees and terrain about 3,000 feet northwest of the departure airstrip. The surrounding terrain was rolling and heavily wooded. The right wing was substantially damaged. Both fuel tanks were about three-quarters full. No evidence of fire was noted. No baggage was found aboard the airplane.

According to the Clark County Sheriff's Office report of the accident (attached), the pilot, who was seated in the front seat, was wearing a four-point seat restraint system at the time of the accident. The passenger, seated in the rear, was wearing a lap belt. The rear seat was not equipped with a shoulder harness. The fuel selector valve was placed in the off position during rescue. The wreckage was removed under the direction of the Safety Board for future examination.

On November 25, 1997, the wreckage underwent additional examination by the Safety Board. The examination revealed substantial impact damage to both wings, all lift struts, cabin area, firewall, engine, and propeller. No evidence of a preimpact flight control system malfunction was found. The flaps were found in the retracted position. Pieces of evergreen branches were imbedded into the right wing tip. The airplane had been modified with the installation of a Lycoming O-360-A3A 180-horsepower engine, tundra tires, and an extended baggage compartment.

Examination of the cockpit instruments revealed that the tachometer time read 1,642.47 hours. The engine fuel primer was found about halfway in the open position and was not locked. The throttle and mixture controls were in the full forward position, and the carburetor heat was in the off position.

The engine remained attached to the airframe by its mounts. The fixed pitch propeller remained attached to the crankshaft and exhibited aft bending and leading edge scoring on one of its two blades. The other blade did not exhibit any notable deformation. Crankshaft and camshaft continuity to the rear engine-driven accessories and all valves was confirmed by manually rotating the propeller. The crankshaft rotated freely and valve action was observed on all valves. Both magnetos remained attached to the rear engine mounting location and did not appear damaged. The left magneto was tested and found to produce a spark on all four leads when manually rotated. The right magneto could not be accessed for testing; it was crushed aft into the firewall. All top spark plugs were removed and examined; they were all gray in color and exhibited oval shaped electrodes. The carburetor bowl was found to contain a liquid that was similar in color, texture, and odor to 100 low lead aviation gasoline. No preimpact mechanical malfunctions were found during the examination of the engine.

The Safety Board removed the airplane's ignition switch and sent it to Teledyne Continental Motors in Atlanta, Georgia, for examination and testing. The examination and testing occurred on December 3, 1997, under Safety Board supervision (report attached). No malfunctions or anomalies were found.

Examination and functional testing of the fuel selector valve in-situ revealed that it was installed 90 degrees counter-clockwise form the correct position of the valve stem. With the fuel selector handle in this position, it was determined through the application of airflow into the fuel lines that the fuel selector was actually feeding from the right tank when the pointer was reading LEFT. When the pointer was selected such that it indicated the OFF position, the selector was feeding from the left tank. When the pointer was selected to such that it indicated the RIGHT position, the valve was actually in the off position. When the selector handle was rotated during the testing, no detents could be felt as the selector was changed from one position to another (Diagrams of correct versus in-situ fuel selector valve operation are attached).

The selector valve was then removed for further examination by the Safety Board. The valve itself was undamaged and remained intact. Functional testing with the use of air into each port of the valve revealed similar results to the in-situ findings that verified an incorrectly installed handle assembly. The valve stem was noted to be square in shape and did not exhibit the D-shape found on the back side of the handle.

The valve itself was then disassembled one piece at a time. The disassembly revealed that the spring retaining washer was incorrectly installed upside down, which prevented the spring from applying pressure onto the slotted detent washer. With the valve assembled in this fashion, the detent feature of the valve was eliminated.

Examination of the airframe records (excerpts attached) revealed an entry, dated January 15, 1997, that indicated a new O-ring was installed in the fuel selector valve. This is the most recent entry of work being performed on the valve that would have required some disassembly of it. The entry also cited compliance with FAA Airworthiness Directive 60-10-08 (excerpt attached) which pertains to checking the detent function and correct rigging of the valve such that the pointer is properly aligned to the placarded fuel tank locations. The entry further states that the detents in the valve were "OK."

The records indicate that the airplane and engine received an annual inspection on the same date of the fuel selector O-ring change. The entry indicated that the tachometer time read 1,611.40 hours (31.07 hours before the accident). No other entries were found subsequent to this entry.

The pilot stated that he did not perform any of his own maintenance on the airplane prior to the accident. He initially stated that he never removed the fuel selector valve handle, and had frequently moved the handle during his flying of the accident airplane on the days, weeks and months prior to the accident in order to manage his fuel load during those flights. He stated that he had never had any previous engine problems as a result of the fuel selector valve position.

The pilot stated that he had been flying the accident airplane frequently during the weeks and months preceding the accident. He stated that he had accumulated about 60 hours of flying time in it during the last 90 days. During that time, he performed some "trim" painting of the exterior of the airplane. He stated that a company called "Northwest Powder Coat" performed the interior painting, including the cockpit side panels. The painting also involved the exterior of the airplane, and occurred about two or three months prior to the accident.

In an interview with the paint shop owner of a business called "Mr. Powder Coat" (record of interview attached), the paint shop owner stated that the accident pilot installed an alarm system for him in February of 1997. In order to reimburse the pilot, the paint shop owner agreed to paint parts of the pilot's airplane. The paint shop owner stated that the pilot and his girlfriend would bring various airplane parts over to Mr. Powder Coat from time to time beginning in March 1997 and ending "about a month before the Evergreen Fly-In." (Subsequent research revealed that the Fly-in occurs during the third week in August.)

The paint shop owner stated that he saw the pilot's airplane at the Evergreen Fly-in, and he stated that he "believed it was all together" with the newly painted parts, including the left side panel where the fuel selector valve is located. The paint shop owner went on to state that he never remo...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# SEA98LA014