N78222

Substantial
None

Cessna 172K S/N: 17257535

Accident Details

Date
Sunday, February 1, 1998
NTSB Number
IAD98LA025
Location
OXFORD, MA
Event ID
20001211X09557
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The pilot's failure to maintain directional control.

Aircraft Information

Registration
N78222
Make
CESSNA
Serial Number
17257535
Engine Type
Reciprocating
Year Built
1968
Model / ICAO
172K C172
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
JOHNSON AVIATION INCORPORATED
Address
POB 673 OXFORD ARPT FED HILL RD
Status
Deregistered
City
OXFORD
State / Zip Code
MA 01540
Country
United States

Analysis

On February 1, 1998, at 1000 eastern standard time, a Cessna 172K, N78222, was substantially damaged after a loss of control during landing at the Oxford Airport (43M), Oxford, Massachusetts. The certificated private pilot and passenger were not injured. Visual meteorological conditions prevailed for the local personal flight that originated at 43M, at 0950. No flight plan had been filed for the flight conducted under 14 CFR Part 91.

The pilot said he departed runway 02, completed a traffic pattern, and returned to land. He said the airplane touched down in the first one-third of the runway. The airplane then began to vibrate as soon as the nose wheel touched down. He attempted to reduce the vibration by applying back pressure to the yoke. He said that after applying back pressure, "...the airplane started hopping on me." The pilot said the airplane bounced twice after the initial touchdown.

The pilot also attempted to retract the flaps during the landing sequence in an effort to increase braking ability. During that time, the airplane drifted to the right, struck a snowbank, nosed over, and came to rest inverted. According to the pilot, "The airplane drifted right and struck the snowbank, probably because I was reaching for the flaps."

The pilot reported that there were no mechanical deficiencies with the airplane. When questioned about the performance of the airplane, the pilot said, "The aircraft was fine." He said he completed a preflight using the checklist prior to departure and did not notice anything unusual.

According to a report from a Federal Aviation Administration Aviation Safety Inspector, "The nose wheel had very little air in it. However, it tested OK [at] 25 lbs. PSI."

The pilot stated that when weather permitted, he flew on a weekly basis. He last flew 2 weeks prior to the accident flight and had accumulated approximately 100 hours of total flight experience.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# IAD98LA025