N955F

Substantial
None

Zwart KIT FOX VIXEN S/N: V95050032

Accident Details

Date
Sunday, February 22, 1998
NTSB Number
NYC98LA068
Location
WEYERS CAVE, VA
Event ID
20001211X09604
Coordinates
38.279678, -78.920150
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The failure of the propeller drive train after the pilot/builder installed an improper drive belt.

Aircraft Information

Registration
N955F
Make
ZWART
Serial Number
V95050032
Engine Type
Reciprocating
Model / ICAO
KIT FOX VIXEN BPAT
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
SALE REPORTED
Address
6000 DOUGLAS DR N
Status
Deregistered
City
CRYSTAL
State / Zip Code
MN 55429-2314
Country
United States

Analysis

On February 22, 1998, about 1600 eastern standard time, a homebuilt Kit Fox Vixen, N955F, was substantially damaged during a forced landing in Weyers Cave, Virginia. The certificated private pilot and passenger were not injured. Visual meteorological conditions prevailed for the local flight which departed from Shenandoah Valley Airport (SHD), Weyers Cave, about 1545. No flight plan had been filed for the flight which was conducted under 14 CFR Part 91.

In a telephone interview, the pilot reported that he had flown over 3 hours on February 22. During the accident flight, he was cruising north of the airport, about 3,800 feet, when he first smelled burning rubber, and headed toward the airport he had just departed from. A few minutes later he experienced a loss of thrust from the propeller, while the engine continued to run normally.

In the NTSB Pilot/Operator Aircraft Accident Report, the pilot stated:

"...Continued to glide to airport at best glide speed. Possibly could have made it but the area just before Runway 05 at SHD is not a good place to try a landing. I chose the field we landed in because I knew I could make this location. The ground was very wet and just after the main gear touched down the front landing gear touched down and buried itself in the soft ground. The nose gear then bent and the plane went nose down and then flipped over up side down slightly to the left side damaging the left wing from the strut to the wing tip...."

Examination of the wreckage revealed that the fuselage was bent, and the right wing was separated outboard of the strut attach point.

The pilot had installed a 4 cylinder water cooled engine, and used a 4 inch wide cog belt to drive the propeller. He reported that he picked the belt used because it was rated for engines up to 300 horse power, and the engine he had installed in the airplane developed 110 horse power. When he examined the belt after the accident, he found that all the cogs had worn off the belt and it would not drive the propeller. The cog belt had accumulated 110 hours at the time of the accident.

A representative of the manufacturer of the cog belt reported that it stated in their catalog that the cog belts were not recommended for aviation applications.

A check with the technical director of the Experimental Aircraft Association revealed they were aware of the limitations of cog belts in aircraft engines. He also reported that the belt used was similar to those used to drive superchargers on racing cars with V-8 engines. The problem with the belts was their lack of ability to absorb the shocks of the power stroke as individual cylinders fired, which became more noticeable as the number of cylinders on the engine decreased.

The pilot reported that he was unaware of any limitations on the use of cog drive belts.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# NYC98LA068