N6235U

Substantial
None

Mooney M20C S/N: 2075

Accident Details

Date
Tuesday, March 10, 1998
NTSB Number
CHI98LA104
Location
WHITE RIVER, SD
Event ID
20001211X09639
Coordinates
43.560726, -100.739341
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

the pilot's delay in applying carburetor heat. A factor associated with the accident was the low altitude at which the pilot was flying which limited his landing site selections when the loss of power occurred.

Aircraft Information

Registration
N6235U
Make
MOONEY
Serial Number
2075
Engine Type
Reciprocating
Year Built
1962
Model / ICAO
M20C M20P
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
EATHERTON DAVID J DBA
Address
HC 80 BOX 460
Status
Deregistered
City
PIEDMONT
State / Zip Code
SD 57769-9501
Country
United States

Analysis

On March 10, 1998, at 1425 mountain standard time (mst), a Mooney M20C, N6235U, was substantially damaged during a forced landing, approximately 4 miles northwest of White River, South Dakota, following a total loss of engine power. The private pilot and one passenger reported no injuries. The personal 14 CFR Part 91 flight was operating on a special VFR flight clearance in instrument meteorological conditions. A VFR flight plan was on file. The flight departed Rapid City, South Dakota, at 1312 mst, with an intend destination of Sioux City, Iowa.

According to the pilot's written statement, after receiving a special VFR clearance he departed Rapid City and maintained an altitude of 500 feet to 1,200 feet above the ground as he followed Interstate 90. The pilot reported that at 1415 mst, he adjusted the fuel mixture to correct a slightly rough running engine. He continued to reported that at 1425 mst, the "...engine ran rough for approximately 15 seconds; I pulled carburetor heat and left it on; the engine quit with the propeller windmilling; I switched fuel tanks back to the fullest tank(right)- no change with airspeed and altitude dropping, I searched for a place to land." The pilot also stated in the safety recommendation section that "...better scan of engine of engine instruments, especially manifold pressure regular application of carburetor heat." The pilot said he suspects it was carburetor ice that caused the engine to lose power.

A Federal Aviation Administration Principal Maintenance Inspector (PMI), represented the NTSB on-scene. The PMI said the engine examination revealed after the air element was removed, the element did not have snow or ice on it. He then used a light and an inspection mirror to look inside the airbox where he found four pieces of ice lying inside of the airbox. Two pieces were the size of a quarter and two pieces the size of a dime.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI98LA104