N331GH

Destroyed
Fatal

Gough-Herrman CHRISTEN EAGLE II S/N: GOUGH 0001

Accident Details

Date
Saturday, March 14, 1998
NTSB Number
LAX98FA112
Location
LAKE BERRYESSA, CA
Event ID
20001211X09698
Coordinates
38.249088, -122.309745
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
2
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
2

Probable Cause and Findings

was the pilot-in-command's failure to maintain control of the aircraft. Contributing to the accident was the improper altitude.

Aircraft Information

Registration
N331GH
Make
GOUGH-HERRMAN
Serial Number
GOUGH 0001
Engine Type
Reciprocating
Model / ICAO
CHRISTEN EAGLE II BPAT
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
HERRRMAN ROBERT J
Address
4557 ROBINSON RD
Status
Deregistered
City
VACAVILLE
State / Zip Code
CA 95688-9348
Country
United States

Analysis

HISTORY OF FLIGHT

On March 14, 1998, about 1343 hours Pacific standard time, a Gough-Herrman Christen Eagle II, N331GH, was destroyed after colliding with water at Lake Berryessa, California. Both the pilot owner and the pilot rated passenger received fatal injuries. Visual meteorological conditions prevailed for the personal flight, and no flight plan was filed. The flight originated at Vacaville, California, on the day of the accident.

A witness reported seeing the aircraft flying about 1,000 feet or less over the lake, roll inverted for about 5 or 6 seconds and then pitch downward, rotate 90 degrees, and impact the water in a near vertical attitude. Other witnesses observed the aircraft during it's vertical descent.

PERSONNEL INFORMATION

First Pilot: The 20,200-hour airline pilot was the owner/operator and one of the builders of the aircraft. He was in the rear cockpit of the dual control aircraft.

Second Pilot: The 14,300-hour airline pilot/passenger was located in the front cockpit.

AIRCRAFT INFORMATION

The experimental homebuilt aircraft was certificated in 1980. The builders were listed as Gough/Herrman, and the current owner/operator as Herrman. At the time of the accident, the aircraft had accumulated about 922.3 total flight hours.

According to the designer/kit manufacturer's representative, the aircraft gross weight in normal operation, pilot plus passenger, is 1,600 pounds. In aerobatic operation, pilot plus passenger is 1,520 pounds. The estimated weight of the aircraft at the time of the accident was 1,516 pounds. The allowable center of gravity (CG) range at that weight in the aerobatic operation is 98.7 to 99.5 inches. The postaccident CG location was estimated at 98.5 inches, or 23.75 percent of the mean aerodynamic chord (MAC).

WRECKAGE AND IMPACT INFORMATION

The wreckage was recovered from Lake Berryessa 9 days after it impacted the lake.

On March 26, 1998, the Safety Board and Textron Lycoming conducted a postaccident examination of the airframe and the engine.

Control continuity was established and examined at attachment points and points of failure. All major components of the airframe, engine, and propeller were recovered and examined.

TESTS AND RESEARCH INFORMATION

During the postaccident examination of the airframe the left aileron bellcrank assembly was removed and sent to the Safety Board Materials Laboratory for examination of fracture surfaces. The fractures were attributed to overstress separation. A copy of the report is attached.

ADDITIONAL INFORMATION

The wreckage was released to the insurance company representative On August 25, 1998.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX98FA112